EPAS CONTROL & POWER HARNESSES
Another OEM system we lost with this "CAN-free" car was the Electric Power Assist Steering, or EPAS. The 2011-14 S197 and 2015-up S550 models all went to EPAS, removing the hassles and dangers of hydraulic power steering pumps / lines / coolers.


This car has a junkyard sourced 2015 Mustang EPAS rack. We then purchased a "stand-alone" harness for the S197/S550 racks from Cortex (the blue/white wires coiled up inside the big red/black cables), then a power harness for this from a late model F150 (the outer coiled cables). This Cortex harness has some sort of circuitry to "trick" the EPAS rack to work without CAN signals. We lose speed input changes and the dash-mounted 3-mode selections using their harness, but I don't really care or notice.


The image above left shows both connectors - the control and power harnesses. The main power cable (#4) is fed from the power distribution through a 100 amp circuit breaker before going to the rack (see above right).

All of this works like a champ - I made a demo video last week, which shows how this works, even with the engine off. This is handy when you are pushing a race car around. We just power on the Cartek kill and - VOOM! - we have EPAS.
CENTER STACK SWITCH PANEL
We don't have the factory HVAC controls or radio - which is what takes up a majority of the center part of the dash. I like to call this the "center stack switch panel", and it is valuable real estate in most race cars. If the driver can reach part or all of this we can add buttons, switches and dials. We started with a cardboard template that Brad cut out, then I scanned that for a CAD version that Jason would ultimately create based on my layout.


For the Center Stack Panel on our Mustang, I wanted to spend a little more time on, really get this dialed in correctly. So many times on race car builds the center stack is a flat panel with switches, dials and ports added over a long period of time without any real long term planning or "cohesive plan". This area adapts as things like a cool suit or new systems that need switches get added (see below left).


I also wanted to use a type of rectangular paddle switch that is common in trucking, marine, and lately race car use. These come in 2 position, 3 position and even momentary push button versions, and can be backlit. I had a gaggle of these I got stuck with on a customer's build he flaked out on, so we had some initial switches we could start with. Long term I will get these custom made with laser etched lettering and symbols that are backlit, but these will do for now.


These rectangular holes are a REAL CHORE to cut out manually, so we created a design in CAD that we could cut out quickly on the CNC plasma table. Brad and I planned out the switch placements early on, along with some additional items: a 7" LCD screen (for a back up camera / lose cam), some USB ports, a digital volt meter, push button start, Cartek main battery kill switch, AiM remote memory card holder, and a control panel / readout for a driver cooling system that would we added later. We also had a comms port for the AiM dash.

Getting the shape of the panel to fit the center stack opening on the S550 dash took a couple of iterations, as did the final sizing of the rectangular switch openings. We also changed the layout of a few items after mocking them up in the car - with me strapped in the driver's seat - after finding the limit of my reach. The 4th version was just about perfect and Brad got that one painted up.


To mount the center stack panel into the dash required some custom brackets, which themselves adapt to the radio mounting area - which is further back and at an angle. Brad whipped these out and bolted them into the partially gutted dash structure. Later on the mounting holes to these brackets was added to the CAD file for the panel, to make later iterations quicker to mount up.


Once we had the layout right Brad wired in the various switches to a DW multi-pin connector, so the whole unit can be unbolted and removed quickly. As you can see above left there is a lot going on behind this panel, but the finished unit (above right) looks clean, purposeful and well thought out. Later on as we add more systems we might need another version but I think this one will last us a bit.


Brad also created a lower mounting bracket at the bottom of the opening, then a horizontal filler panel that that ties the bottom of the center stack panel to the lower console - fills in a section that is normally a plastic storage cubby. And that big blank section at the bottom of the panel is for the driver cooling system controller, which we will add later (basically an air conditioner for water that will go through a driver worn cool suit).

This is the completed center stack switch panel, along with the functional 7" LCD screen for a back up camera - which has been surprisingly useful on this car! I use this in my street car daily drivers, and every single time I back up this Mustang it gets used. With Halo style racing seats and a HANS device on this will be a welcomed addition for visibility behind. I bought this screen ages ago and I think it was about $50. The license plate frame with included camera and LED light was about the same amount, so for $100 we have a useful addition - an more D&E points for Optima, haha!
AIM MXG 1.3 DIGITAL DASH (DOES NOT WORK WITH HOLLEY EFI!)
This section of the project was an unpleasant surprise - which we learned about after the fact - Holley doesn't support any other aftermarket digital dash. AiM Sports made it sound like they worked with Holley HP and Dominator EFI systems, so I purchased an AiM MXG dash, but that was a lie. There is a nerfed Holley output that supposedly works on RacePak digital dashes, but you lose ~75% of the Holley data channels with that protocol.


We spent a chunk on this AiM MXG and the remote SD card holder, and spent a chunk of time mounting it all - all for naught. I really like AiM dash units because they (can) log data and I am familiar with their data analysis software. These units also have an industry leading lap timer and predictive lap readout feature. Words cannot describe how pissed off I was at the end of this section of work to realize that we HAD to use a Holley dash...


I will show the steps where Brad made the mounting brackets and panels - because we re-used all of this to mount the Holley digital dash. I wanted the steering column plastics installed, to keep the interior looking "finished" for a few racing classes we had in mind. The trimmed hole above fits the AiM and Holley screens.


I had purchased missing items like the factory gauge bezels, then Brad made a "gauge block off" panel starting with cardboard and going to aluminum. Sections of the angled and round bezels had to be modified to fit this blanking panels.


Mounting brackets for the blanking panel were added inside the back section of the gauge bezels, then the AiM dash template was used to transfer the mounting holes for this screen.


I was happy with the finished install, but very UNhappy to learn this screen won't work with any Holley EFI system. I will use a remote AiM SOLO lap timer for use on track for now, but that is more clutter on the windshield I was hoping to avoid.

We're not giving up all hope, however, and have a CAN integration specialist working on a custom box to help the to devices talk together. Its much harder than just "sniffing the CAN signals", but I will cover this in more detail next time - if we can make this work.
DASH INDICATOR LEDS
One of the things that can happen when you have a LOT of sensors and data displayed on a digital screen is DATA OVERLOAD. So we have some warning indicator LEDs we planned for and I purchased. These cover things like low fuel level and ABS warning lights, but also left and right turn indicators, high beam lights, and even Reverse light indicator. These have already proven useful in testing.

I purchased 6 of these units online at $8.95 each and Brad got to work on the layout and placement of each, testing with me in the car for each one.


These all are wired into another DW 12 pin connector for easier panel removal and work. The first one to be wired in was the low fuel indicator from a level switch in the top of the Radium remote surge tank. This was an optional item when purchasing the surge tank and lets you know as soon as the tank goes from "full" to just a bit under - which means you have about a liter of fuel left. This is a "BACK OFF THE LAP AND PIT RIGHT NOW" light.


We have also added a Reverse solenoid controller and when the transmission is shifted into Reverse the "R" indicator on the dash lights up. We have 4 other indicators that we will wire in as time allows, after the dyno testing is complete.
FLUIDS INSTALLED + STARTER BUMPED
By Mid-November 2022 we were ready to start adding fluids and bump the starter, crank the engine, and check oil pressure. This would also be a full plumbing system leak test.

I decided to use a Motul break-in oil for the first dyno test, which we would change out for proper Motul 5W50 Ester synthetic before the first track test. We needed THREE GALLONS of oil to fill the oil pan, filter, oil cooler and Accusump.


We filled the cooling system with distilled water and a touch of anti-freeze. We used a cheap AC Delco DOT3 hydraulic fluid for the brake and clutch systems - anticipating some small leaks, which of course did happen. This will be flushed and bled with proper Motul RBF600 or 660 once the initial dyno work and test driving is completed.


Filling the diff cooler system was a challenge. We had a "T" fitting high up in the system with a cap, just for this purpose. But since the cooler was above the diff housing, we would have to do a calculated fill. The pump acts as a check valve so once fluid gets pumped into the cooler is stays there (again, this is by design). We had to run the pump to get everything full, until it was coming out of the top hole (the normal fill line). Then added the amount that goes into the cooler. Doug used a long funnel and added the 3.6 quarts of Valvoline 80W90 diff fluid (Motul Gear300 was out of stock globally) and some Auburn Gear limited slip additive.
FUEL PRES REGULATOR MOVE, LOAD START-UP TUNE, CHECK SENSORS
One of the things Brad noticed when he want to add some sensor wiring was that the Aero fuel pressure regulator was in a tough spot to reach and had some plumbing that got a little to close to the exhaust header. After looking at this closely I agreed and set him loose.


After making a new bracket he relocated the regulator, re-routed the hoses, and made one new Fragola hose. That keeps the regulator as far away from the headers as possible without putting it too far from the fuel rail to be useful.


We had somehow missed adding a MAP sensor, so we ordered the correct LS6 style from AC Delco. There are two options for the one O2 sensor on a Holley - NTK or Bosch. We also ordered and installed the wide band Oxygen sensor, the NTK "0.9 Lamda" unit (for NA engines), from MAD Racing.
FIRST FIRE TESTING
All sensors were installed and wired, all fluids filled, now the battery was charged up. The starter had been bumped several times, even cranked, to fill fluids into the oil system.


We took the start-up tune from our tooner and Doug loaded that to the Holley ECM. We added fuel and cranked... checked fuel pumps, checked spark plugs, but it would NOT start.


We had to triple-check major sensors, like the crank sensor. We verified that I had ordered the right 58X reluctor sensor and that we had a 58x reluctor on the crank.


We were getting weird faults and then checked the distance from the crank sensor to the reluctor wheel, using a socket, marking the depth and checking against the sensor. That wasn't it.


After a two days of testing, checking, new tunes, phone calls and more cranking we found the issue - the Holley ECM will LOSE THE TUNE sometimes when the battery voltage to the computer dips below 10V when cranking. And sure enough, the battery would drop nearly 2 volts cranking (see above images) and we had to reload the tune and re-run the TPS setup wizard. This isn't a bug its a FEATURE, haha! (this is a MAJOR bug Holley... major).

On November 18th, 2022 we finally figured out the "tune disappeared" mystery and got it to fire up, which you can see in this ugly video. We still had a massive vacuum leak and the idle was high, but that was found later and the idle RPM calmed way down. We needed to bleed the brakes and clutch systems, but hearing the engine run was huge.
SPL PARTS REAR ARMS
If you followed our 2018 Mustang GT development thread you know that we had some of the earliest SPL Parts for the S550 Mustang on that car. We are an early tester stuff for their parts, and I know Sean and Turner from that company well - they are the current NASA Texas Time Trial directors and TT racers we see on track.


They sent us these upper rear control arms right after they went into production in 2022 and they look amazing - even with a schlub like me "modeling" them. Gorgeous parts they design in-house and have machined here in Texas, with some parts on their own CNC machines at their new facility. I was more than happy to test these out on Trigger!


It didn't take Doug long to swap out the stock, heavy steel upper arms for these new adjustable units. This will allow us to finally get more than -2.2 degrees of rear camber! (We ended up at -3.2 deg when it was aligned - see more below).
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