

With the evidence clear that the rear caliper failure made me go four off and crater the cone at Track Test #2, it was time to fix the damage to the fiberglass front nose (see above left) - a fairly large crack in the lower splitter piece. We picked up a fiberglass repair kit with some woven glass fiber cloth, resin and hardener.


After sanding the area to give the resin something to "bite" into, Brad added the glass cloth on the inside and outside of this crack. When the resin setup and was sanded, it looked pretty damned good after the first application. "Good enough - paint it!"


With a couple of coats of SEM "Trim Black" paint it was a perfect match and a hidden repair. Nobody ever needs to know...


Last up in repairs this round was a cover for the giant Magnaflow mufflers in the trunk. At this point I held out hope we could fix ALL of the issues, get the car sorted and fast, and make it to the Oct 15th SCCA Time Trial Nationals event at NCM. After asking for some scrutiny, one of the SCCA TT board members told me that the open trunk might get tagged in Max 1.
We laid out plans to make an aluminum metal cover for the mufflers. Brad made this in two pieces, and started with the forward portion shown above - from a cardboard template. He left ample cut outs for all hose pass throughs, of course. We weren't looking for an air tight cover, just a best effort to close up this hole and prevent hot mufflers from getting touched directly by curious ding-dongs when the car was in Impound with the trunk open.


The rear section is this raised 3 sided box, made from a single sheet of aluminum from another cardboard template. This has flanges at the front and sides to attach to the rest of the trunk, with rivnuts and bolts connecting this piece in place.

The finished cover looks really good and we never had to remove this during the 2023 season after this was added in late July. But it could quickly be removed if we needed room for service. Probably should have installed this sooner but we have been knocking down problems at break neck pace.


We had OEM fender liners in place but they were not attached to an undertray, because... well we hadn't gotten around to installing that yet. See, on this radical of a new build we were always looking for leaks and other things that an undertray or splitter would hide. Luckily we never had any leaks, but the floppy fender liners had rubbed up against the front tires, unsupported at the bottom. Running without the undertray we had on hand was a mistake, and adds a LOT of drag. It also makes our brake cooling deflectors much less effective. We just... had so much to do between every outing!


The Anderson Type ST fenders came with these fiberglass "extensions" that filled the gap the 3/4" wider fenders needed, and now was the time to install those + add some aluminum supports for the fender liners, as we were still not ready to install an undertray or splitter just yet. At least with this bracing the OEM + Anderson fender liners wouldn't be flopping around and catching the tires.
UPGRADE TO MSD ATOMIC INTAKE + 103MM TB
Now this was planned for a number of weeks, but I was very hesitant to implement this because... well I hated to give up ALL of that hard work and potential power of the modified Trinity intake and 112mm throttle body. But damn, y'all this car was impossible to drive smoothly and quickly. We thought long and hard about any number of "short runner" yet taller intakes, like the FAST LSX HR, Holley High Ram, or any number of Hi-Rams with modified uppers. All of those would require cutting a LARGE hole in the carbon fiber hood, creating a visual impairment. We still might do this, but not if it means cutting the hood and looking over a giant mail box!


At this point we had to punt and go back to a "known good" intake and throttle body - the LS7 MSD and 103mm Nick Williams DBW throttle body. We knew it would give up SOME power, but we also had seen too many HPR built 454-468" LS7 engines with this intake make 630+ whp.


I had to identify what exact ID 1050 injectors we had in the car to be able to order the correct MSD fuel rails, as the rails we had on the Trinity were unique to that BTR intake. After identifying the right fuel rail kit that was ordered as well as the MSD Atomic LS7 plastic intake.


We had a 4.5" straight connector on the 112mm throttle body so I tracked down a 4.25" to 4.5" silicone adapter from HPS, to go to the new smaller 103mm TB and join the existing 4.5" cold air. With all of the parts ordered, Brad pulled the Trinity for the last time...


We have purchased a number of these MSD Atomics, and while I hate the way they look and it sucks to have to fix so many of their crappy manufacturing defects, I cannot ignore the simplicity and power these make. This is THE most powerful plastic intake on the market for LS7 heads, bar none. It wins every test when they are put up against any plastic OEM style "long runner" intake, and damn near all of the shorter runner intakes, too.


I ordered the correct fuel rails for this intake and our injectors, but the NW 103mm TB was out of stock at the only supplier, SDPC. Well we had a brand new one on the LS2 C6 - which was about to go for sale - and we stole that one for a few weeks until the supply came back online. That cathedral port LS2 had the best intake for THAT cylinder head style - the FAST 102 LSXR - which wins all of the intake test for cathedral port LS engines. Don't ask me why but it edges out the MSD Atomic for that port, but not the LS7 style port we have on Trigger's 454" engine.


I got the plain "black" unit and Brad got to work cleaning up all of the jagged plastics. NOTE: do not expect to install this in a day, oh no. You might spend several hours removing casting flash, sanding down imperfections, and even adding epoxy to get the base to seal correctly to the upper cover. We highly recommend that you SMOKE TEST this intake before you put it on your engine. We have learned this the hard way - these can leak air from a dozen different places.


So that was mocked up, and the fuel line changes were done, but we still had some work to do. I just... hate the way these intakes look, and the long 8.5" intake runners would definitely shift the peak power down from 7000 likely to 6400-6600, like these always do. Sure, it might gain some "area under the curve" (ie: mid range power), but damn - I almost don't WANT any more mid range power (in the autocross it would rev up to about 4500 rpm in 2nd gear and just blow the tires away easily).
Look how much wasted space above the top of the intake we have just to the strut brace? GRR... I know we can do better than this, but let's move along here and get this one running and re-tuned and dyno'd.
MORE TROUBLE WITH STEAM VENTING + "FITTING" THE MSD
We had the intake, fuel rails, and fuel plumbing wrapped up with the new MSD on August 1st, but it took fully a WEEK later to get all of the right pieces for the 4 corner steam vent system. The intake was not bolted down to the heads as we were waiting on the steam vent kit.


We fought putting together a real 4 port steam vent install on the LS2 in the C6 and this was no easier. The last MSD we did on a car was backwards and in a different chassis, so this kit made for this exact intake should work, right? Ha! Brad put it together per the instructions, as seen above right.


The "tower" that sits at the front of the driver's side head near cylinder 1 is really hard to configure right to clear the MSD, so Brad drilled and tapped the TOP of this cylinder. Then a 90 deg fitting went into that and the old hole was plugged. This allowed the two braided -3 AN lines to route back along the top of the Katech valve covers and under our fuel rails to get to the back two steam ports on the backs of each head. It was just packaging challenges, nothing new.


Next up was a considerable amount of work that needed to be done to make the intake actually fit this Brodix BR7-BS head. The original intake port gasket O-rings that came with the intake were ALL pinched from the get-go, so those were also replaced. The gaskets these come with are just trash.


Brad spent a couple of hours sanding down this lower edge on both sides to work with this cylinder head. Don't know why this needed to be done, but its just a common issue with the MSD. Lots of taping, sanding, vacuuming, cleaning, and test fitting.


Once the intake fit properly the bolts were finally installed and carefully torqued per MSD's instruction sequence. You can see the close-up of the final, modified steam vent tower above right. The old routing would not clear that corner on the intake - between that, the fuel rail and the valve cover, it gets tight.


The final exit for the steam vent tower goes to the same line on top of the radiator hose, as shown above right. Then it was time to top off the coolant system and let it run for a bit to warm up and open the thermostat.

This short video shows the engine running with the old tune on the new intake. It would need a complete re-tune with the new throttle body and intake.


The cooling system was pressure filled with this cap adapter and compressed air system. The existing 4.5" ID cold air system lined up easily with the new reducing coupler at the smaller throttle body - at least that went smoothly. That got us ready for the dyno time, but we had only two days until the next SCCA Time Trial and I needed a WIN. I was really down on points with borrowed cars.
DYNO TEST #4 - AUG 8, 2023
We only had about 4 days until the next SCCA Time Trial and all of the install and modifications to the MSD took longer than we had hoped. We had no time to schedule our normal tuner Jon, but luckily a former Vorshlag team member was now doing tuning work and was familiar with the Holley Dominator EFI. He met us at the Vorshlag shop on August 8th (or August 2nd, we have some record discrepancies) and we hauled the car to X-Factor Racing down the road in Princeton to use their DynoJet 224 chassis dyno.


It was staggeringly hot that day, with recorded temps between 97-104F deg in the dyno area. We worked through the heat and the cooling system on Trigger barely registered 195F after a dozen pulls. We ran into some issues with the inductive lead on the roller, but we made several 620 whp pulls in a row and quit adding timing and fuel when things dropped off.

Donnie tuned the car on the dyno then worked with me on driveability issues with a little back roads of Mexico street testing. The idle was still a bit lumpy but the throttle tip in and drop out no longer jerked the car around, so I was hopeful it would be easier to drive on track. I made this little video above after we got back to the shop.

We got this weight check August 10th, after the dyno tuning and the last of the task list and right before loading it into the trailer for the SCCA Time Trial Aug 12th at MSR Cresson.


Loaded up in the trailer, with the BRZ going on the open trailer behind the Maverick once again. This would the hottest race of 2023! Luckily both cars had functional driver cooling systems installed.
SCCA TT, MSR 1.7 CCW, AUG 12, 2023
This was our second SCCA Time Trial in Trigger, and I hoped it would go better than the 1st time - where I scored a dismal 3rd. If we had any prayer of winning Max1 for the season I HAD to score wins here and at every other event for the year. We towed two trucks again and were setup and ready with plenty of time before the TT meeting. Long day - we didn't leave until 4:30 pm when the truck's temp gauge showed 112F deg, phone showed 106F.

This was by far the hottest Time Trial I had ever done, and I did all 4 sessions - because I'm a masochist! After the first session (free for all, no times to grid by) I was gridded P2 for Session 2, behind Stan Whitney's 2020 GT500. We had both run a 1:19s, he had a 1:19.6 and I had a 1:19.8. We both ran 1:19.0's in session 2, with me just a hair quicker. Session 3 I ran that 1:18.9 and he had a 1:19.1. 4th session he went to grid - to dare me to go out, too! - and I ran a 1:19.1 to Stan's 1:20 - heat soak finally getting to the supercharged GT500. This was a crazy close battle all day!


Session 1 was 83F, Session 2 was 85F, then Session 3 was 95F, and Session 4 was 103F! My driver cooling system was low on fluid so it stopped working - I didn't realize that until later - we now have a "top off" procedure before every event. Also, instead of disconnecting my cool shirt vest every time I get in and out of the car, I leave it connected and put it on while seated (so it doesn't lose water at the quick connects each time). The throttle response was much better with the smaller 103mm TB but it was still VERY easy to lose rear grip in 3rd gear simply from acceleration. You can see a BIG tail slide drifty boi move at the end of this video...

That was my session 3 with one good hot lap and one junky, slidey lap. A very prepped GT3 RS 911 (somehow in Max3??) snuck ahead of me in Session 3 - he ran a 1:18.7 to take FTD. I don't ever want that to happen again!

Trigger was running well, still doing the low oil pressure trigger thing, and it would only do it in Lap 2+ a lot, with only some triggering in the last triple left hander on Lap 1. So it's still there, but manageable. I had to really push hard on lap 1. First 2 sessions I didn't get good temps in the tires and/or had traffic to deal with, so my best laps were on hot lap 2 - when these A052 tires were boiling and the oil pressure trigger was the worst.


In Session 3 I was fastest overall so P1 on grid, which meant I could set the pace on the out lap, and got some temp in the tires and hit it hard on hot lap 1, which was my best. This way I avoided the oil pressure issues of lap 2 and beyond. Track temp was 126F as measured when I came back in from that session. Not ideal.
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