Announcement

Collapse
No announcement yet.

Vorshlag Shop Truck - 5.3L SWB GMT800 (Truck Norris!)

Collapse
X
  • Filter
  • Time
  • Show
Clear All
new posts

  • Fair!
    started a topic Vorshlag Shop Truck - 5.3L SWB GMT800 (Truck Norris!)

    Vorshlag Shop Truck - 5.3L SWB GMT800 (Truck Norris!)

    Project Introduction, April 2, 2013: For the past 7 years or so I've been using one truck to both tow our race trailer as well as to serve as the "parts runner" for picking up and dropping off pallets of parts to various local vendors. Initially this was a 2001 Chevy crew cab 1500HD 3/4 ton with a crew cab and a 6.0L V8 engine towing an open trailer. When we stepped up to a 38' enclosed gooseneck trailer I also stepped up to a 2006 Dodge 3500 5.9L Cummins MegaCab SRW 1 ton. Neither trucks were modified except for very minor cosmetic updates or things like better tires or aftermarket trailer brake controllers. They were both extremely clean and well detailed, but I do that to all of my vehicles. Still, they were big boring trucks that I ended up daily driving with for many years. If you daily drive in a 3/4 or 1 ton truck you know how big, heavy, and slow they are. After many years of wielding these behemoths through traffic it... just kinda sucks.


    My previous tow vehicles/shop trucks: 2001 Chevy 1500HD 2WD 6.0L (3/4 ton) and 2006 Dodge 3500 Cummins SRW (1 ton)

    The Dodge was still dead reliable but was racking up the miles, so in January of this year we custom ordered a 2013 Ford F-350 dually diesel and put the Dodge up for sale. I was tired of driving around almost 100% of the time on the street in giant trucks and I was bound and determined to not let this new dually become the "shop truck", used for running parts around town plus my daily commute. Somehow I always end up putting 20K+ miles per year onto my "tow trucks", with most of that not towing a trailer.

    Another big problem with using one truck for both towing and "driving around" is that the new dually is so wide it cannot be driven through a typical drive thru, like at a bank - which I end up doing once or twice a day. It is also a crew cab long bed, the longest possible configuration for the F-350, so the wheelbase is a staggering 172" long. But the added wheelbase and width of the dually are actually better for towing a big enclosed trailer - it adds stability, cargo room, passenger room, and the long bed allows the front of the gooseneck to swing and clear the cab. Ask me why that matters sometime and I will tell you a story about the trailer meeting the cab on the Dodge the first time I towed with it and tried to make a U-turn, which had a shorter 6.5' bed...

    MEET OUT NEW SHOP TRUCK


    The 119" SWB GMT800 is so much easier to park, maneuver and drive

    So for our shop "parts runner" truck I wanted to buy a separate vehicle, but go almost the exact opposite way than the F350 dually: this one would be a 1/2 ton truck, so it would be lighter, handle and ride better, and have a much narrower chassis built on the shortest wheelbase possible. The answer I came to was a proven workhorse - the GMT800 chassis - with the shortest of 4 optional wheelbases at 119". This wheelbase is a staggering 54 inches shorter than the F-350 dually will have. GM made literally millions of these so I figured it would be easy to find exactly what I wanted (ha!).

    What is the GMT800? http://en.wikipedia.org/wiki/GMC_Sierra

    The GMT800 generation of 1/2 ton trucks was built by GMC and Chevrolet from 1999-2006 model years (and even some 2007 models). This truck was a radical deviation from previous 1/2 ton GM trucks with a host of new technological innovations. One big improvement was in chassis rigidity, as the 4 wheelbase variations for the frames were made with the hydroforming process and tubular cross beams, instead of stamped steel pieces. This was a technology originally developed for the C5 Corvette, which is explained below.

    Hydroforming is a specialized type of die forming that uses a high pressure hydraulic fluid to press room temperature working material into a die. To hydroform a vehicle's frame rail, a hollow tube of metal is placed inside a negative mold that has the shape of the desired end result. High pressure hydraulic pistons then inject a fluid at very high pressure inside the metal which causes it to expand until it matches the mold. The hydroformed metal is then removed from the mold. Hydroforming allows complex shapes with concavities to be formed, which would be difficult or impossible with standard solid die stamping. Hydroformed parts can often be made with a higher stiffness to weight ratio and at a lower per unit cost than traditional stamped or stamped and welded parts.
    Ford quickly countered this new technology with hydroformed frame rails on the 2004-current F-150, too. Lots of cars now use this technology in frame sections and other formed steel and aluminum components.



    The GMT800 chassis also had several other firsts: 4 wheel disc brakes, 4 wheel ABS, LSx based engines, electronically controlled 4 speed automatics, tighter panel gaps and better aerodynamics, and much more. With updated electronics and better fuel injection these were more efficient, more powerful, and more reliable than any previous generation of GM truck. These have evolved into the GMT900, which covers 2007-current 1/2 ton trucks with cosmetic changes and some other small improvements.

    I looked at other 1/2 ton trucks, but the newer GMT900 was a bigger truck that got both taller and heavier, and the only 1/2 ton Fords I cared for were the $55,000 Raptors. The 3rd generation 1/2 ton Dodge from the late 1990s/early 2000s era is notoriously less reliable than the redesigned 2009 4th generation Dodge Ram. In addition to the massive improvements in reliability, brakes, drivetrain and chassis, I just liked the look of the GMT800, especially the Regular Cab Short Bed 119" short wheelbase version (aka: RCSB).


    Left: The newer GMT900 is taller than the GMT800. Right: I made this WANTED poster and posted it on Facebook

    After looking off and on for 6 months and striking out, I started seriously searching after I ordered the F-350 and sold my Dodge 3500. The Dodge sold too quickly and the F-350 took longer to get built, so I was left without any truck for about 5 weeks. During that time I racked up 2000 miles on my 2013 Mustang GT, nearly doubling the odometer reading, just running parts around town. So this sort of sped up my search and I got more serious in my efforts. There were a lot really poorly written ads on Craigslist and too many car dealers that lied about what they had (V8s that turned out to be V6s, "Excellent" bodywork that ended up being trashed, lots of bait-and-switch trucks that didn't exist when I got there). All told I looked at about 600 online ads, a dozen actual trucks in person, and had tons of people searching for this truck for me. Somebody here at Vorshlag actually found this 1999 GMC Sierra 1500 below, and since it was located way out in the boonies I was the first person to come look at it. After a look to see that it was really what he stated (SWB, 5.3L, 2WD), a quick test drive and some haggling I bought it on the spot for cash. Big thanks to Jason McCall for going with me to get this truck (plus looking at several other turds with me in previous months!)



    This example has "some miles on it" but the condition and price were too good to pass up. This has always been a Texas truck so it has no rust, and it had never been wrecked. The optional engines include a V6 and two V8s (4.8 and 5.3L), and this one had the much rarer 5.3L LM7 (same engine that we used in the GRM Challenge E30 V8!). It uses all of the same LSx parts we are familiar with and comes with the iron block and aluminum heads and was rated at 270 hp (there were also 285 and 295 hp versions in later GMT800s).

    I picked the GMC over the Chevy Silverado simply from the looks - the GMC's factory front headlights and grill are more pleasing to me than two Chevy versions, made from 1999-2002 and 2003-2006 (but the aftermarket "billet grill" on this one has got to go). The RCSB trucks were much harder to find with V8s and 2WD than I had figured, as these are popular with the hot rodding and even drag race crowds. The lines are pleasing so the pimps hoard them, and the weight is lower than the other 3 wheelbase options so the drag racers gobble them up, too. Yes, people in Texas drag race these SWB GM trucks, in large numbers - don't ask me why.


    Don't try this - you can overload a 1/2 ton truck when you put 3000 pounds in the bed! Luckily I never haul loads this

    Of course I don't expect everyone to agree with my truck decision, but this wasn't some random decision and the purchase has been made. I'm sure you have had great luck with other trucks, or have a horror story about someone else's GMT800, too. But I have owned a GMT800 and it was dead nuts reliable - as have many other friends I trust - so I just wanted to get the short wheelbase version and see how it drives. And after a couple of weeks of ownership I found that it drives VERY WELL. This truck is super easy to drive in traffic, ridiculously easy to park, it navigates the bank drive-thru effortlessly, and it hauls a pallet well. I've already over-loaded it once, with a 3000 pound load of hardwood flooring, so we have a few things we need to improve to better serve as the "shop truck".



    This truck has an amazingly clean interior with the upgraded "LS" package, so it has the power options but is still cloth. The split bench has the console/jump seat, for a 3rd seating option in those instances where I need to carry another person (rare).

    YES THE WHEELS ARE UGLY

    The truck is mostly stock, which I wanted, but someone added a few modifications. Most of the mods are coming off, some already have been replaced or "fixed". The "Boss Motorsports" 20" chrome wheels are not at all my style, but we do want to show off some of the other products we sell on this and all Vorshlag vehicles, so it will likely get something like Forgestar wheels in a more reasonable 18" diameter. the smoked tail lights are both ugly and dangerous and will be changed quickly. The Edlebrock headers that were added by a previous owner have some leaks so we have a set of American Racing Headers 1-7/8" full length stainless steel headers coming soon. The after-header exhaust is a mess and will all be replaced with some typical Vorshlag custom exhaust work.



    It looks like it already has been lowered a bit so we will change the wheel/tire package and reevaluate that. To help with towing (we need a back-up tow vehicle for short, local towing of cars on an open trailer) and improve the load capacity of this truck, we will add some load leveling airbags too the rear. There are also better OEM brakes we can use from the GMT800 chassis, too: the 1999-2004 GMT800 had 12" front discs with a single piston caliper. The later 2005-06 GMT800 extended cab trucks had a 13" rotor and twin piston PBR caliper. Could be a cheap and easy upgrade that utilizes heavier duty, OEM parts? We will do the research, pick up some new 13" brake parts and see what it takes.

    I always assume some of you reading this will have some experience with the changes we have in mind, so feel free to chime in with tips and advice; hopefully it will be more than "God, those wheels are ghetto!". Yes, there are some aftermarket parts on this truck that are not to my liking - the price was good enough to help me ignore most of these these small issues.

    I will update this thread as we repair, upgrade and tastefully modify this truck for our "shop truck" use.

    Thanks,
    Last edited by Fair!; 07-03-2017, 09:05 AM.

  • Fair!
    replied
    continued from above

    REAR SWAYBAR AND AIR LIFT AUTO LEVELING SYSTEM INSTALLED

    In late 2022, after waiting about 18 months (this was "pandemic supply chain" time) two items finally arrived - the Addco rear swaybar and the Air Lift compressor and automatic leveling system for the rear helper bags we installed in 2020. I thought this stuff would NEVER arrive. Customers always complained about waiting on parts but WE ALL HAD TO WAIT back then.



    In late November 2022 we made time to bring the Silverado into the shop and tackle the installation of these two items. While we were in there the leaking rear pinion seal was replaced - that had less than 100 miles on it, but something was pinched during the Eaton LSD + 3.73 gear install. It is a relatively easy fix.



    The rear swaybar install was relatively painless. It uses U-bolt clamps at both the axle (to mount the bar) and the rear crossmember (to mount the endlinks). i made sure we had the right pivoting friction at the mounts and we moved onto the Air Lift components.



    It was time to get the rear airbags plumbed to a proper compressor and leveling system - we had been just topping up the air from a Schraeder valve behind the rear bumper cover while we awaited this kit to arrive. The compressor was installed behind the left rear wheel, up inside the frame rail (see above left) on rubber isolators.



    The Air Lift leveling kit includes the compressor, new lines, push lock fittings, and an air gauge for both rear bags - with an up / down controller on the gauge. We discussed where to put the gauge and I wanted it in the center roof console. I'd lose my sunglasses holder pocket, oh well.



    I had this new tech make an aluminum panel that bolted in place of the storage pocket in that upper console. He ran power to the gauge for lighting and control. He used constant 12V power, which we figured out after he left. This would trigger the compressor every few days to top up the bags for the ride height / pressure we picked. If you happened to walk by the truck when the compressor topped up a bag it would make you jump! It also drew down the battery needlessly, but Brad fixed that in 2024.




    It might be hard to see but the helper bags raise the rear up so this truck can carry loads. It also keeps it from having a reverse rake, which it did before we added the bags. The controller notes the pressure in each rear bag and tops them up after you start the truck (now that Brad has the system wired to switched 12V power), so it always sits level - no matter what load you have in the bed. Pretty slick!



    Another quick upgrade was this front radiator support cover - we didn't have the right one for a while, but I bought a 2003-07 style and that went on and completed the underhood transformation from the 1999-2002 style. There are a lot of differences!

    DASH CRACK FIXED

    When the truck came back from paint in April of 2021 the dash had a huge crack in it - the sun had gotten to the 22 year old plastics and did the damage. It happens often to trucks of this era, but luckily there are good solutions to fix this. It took us a while but we eventually got to this repair in January of 2023.



    Jason found this Dashskin repair kit made for this exact truck model / year / color and I ordered it. Several hundred dollars but it really fits perfectly, so it was worth it.



    This was a complex job that required attention to detail. The existing gauge panel cover had to come off, as well as the various HVAC vents and some other items. Then the OEM plastics that this covers up had to be cleaned, primed, and adhesive added.



    With the new dash skin installed, a soft cover was placed over it and weights gently set onto the top face to keep it positioned while the adhesive setup over night. The next day the grab handle and vents were installed and the dash looked better than new!



    I had noticed a slow power window on the driver's side so I ordered this new regulator which was installed at the same time. These are fairly common wear items so there are a lot of good repair parts. Just a fiddly job that has to be done on 20 year old GM vehicles.

    ANOTHER NEW BATTERY AND A TUNING BREAKTHROUGH

    The tuning issues persisted and I quit letting my technician mess with the truck - days and days of time wasted, and it just wasn't much better. In 2023 he moved on, then we got really busy working on Trigger, my 2015 Mustang race car with an LS swap. That car kept Brad pretty tied up all year, and once we got it on track I ran it more than 20 times that season. Meanwhile the Silverado just sat in my barn for the better part of a year. The yellow top Optima was dead as a door nail when we went to go move the truck, and all attempts to revive it failed. It was a $279 paperweight which was likely used ~15 times to start this truck.



    This is long after I had lost my patience with Optima batteries and I had started buying old school wet cell batteries from O'Reilly Auto Parts - these units cost only $120 and have a 7 year warranty. Every single race car that had an Optima battery had issues, but after we installed the "Super Start" lead acid units, the problems magically went away. I'm talking about 6-7 difference street and race cars. We replaced the battery in the Silverado in January 2024 in preparation for a custom dyno tuning session at LG Motorsports for this truck.



    And in February of 2024 I had a scheduled slot for tuning this truck there - the 6th tuner to attempt to fix the weird idle issues, the shifting issues, and some other drivability things. Sergio at LGM did his magic, like he has on many other LS powered cars for us in the past, the the truck was TRANSFORMED. It runs great now, starts on the first crank, and made good power and torque numbers. The shifting issues are sorted, the truck drives great in normal street driving situations, and if you open it up the HPR built 5.7L LS engine will rip the rear tires to shreds. It is finally perfect, finally DONE.

    WHAT NEXT?

    I really don't know what I would do with the truck now. I use the Maverick on my 2-3 weekly parts running trips, and even though its 22 years newer it is worth less than what we have in this 2000 Silverado. In the end I spent SO MUCH MONEY on this truck it is insane. I am now afraid of getting it damaged in some stupid fender bender, and even with declared value insurance, I know I'd take a bath if something happened to it (like when the tree limb fell on it).



    It is just sitting around waiting for me to drive it, but of the 4 trucks it is the last one I go to for parts deliveries or transporting anything. It is wasted in my care now - so I will create a classified page and put this one up for sale next. I will post up here when it is sold. Thanks for tuning in for the last several years everyone!

    Cheers,

    Terry @ Vorshlag

    Leave a comment:


  • Fair!
    replied
    continued from above

    EXHAUST ROUTING CHANGED

    There was a long term exhaust leak that really bugged me. By August of 2021 I was frustrated and this massive exhaust leak not only sounded bad, I was worried it was effecting the tune (it wasn't).



    This was the same Stainless Steel long tube 1-7/8" primary / 3" collector headers, center exhaust and cats from American Racing Headers that were on my former GMC pickup that we first purchased and built more than 11 years ago. The slip fit connections that ARH likes to use always end up leaking, and they leaked on BOTH trucks.



    We got the truck on the lift and I showed Zach (above left) what I had in mind. He directed our welder at the time Mason (above right) on some of the welding, then Zach did more stainless welding on the finish work.



    The 2-into-1 merge that used to be back by the massive Magnaflow 3" muffler was moved forward, just behind the transmission crossmember. Then a 3" stainless steel V-band clamp was added in place of those damned slip fit clamps. This sounded SO much better without the constant exhaust leaks, but the truck still had a weird tuning issue - which we had been chasing ever since the 5.7L engine was swapped in.

    ELECTRIC FAN RELAY UPGRADE

    August in Texas is as hot as it gets, and if you have functional air conditioning in your vehicle you use it at all times in this state from June-August. Well I took the Silverado to drop off / pick up parts across town in August, and had another coolant "episode".



    As soon I got a warning light for coolant temp, I looked down, saw 230F degrees. I immediately shut it off and parked. Then I lifted the hood to let the engine cool off and added water to the overflow tank when I could get the cap off. Once at the shop I checked and the big Ford Mustang 5.0L electric electric fan we transplanted to this truck was not working. Brad found the issue quickly - the fan relay had failed at the plug. Instead of replacing this again (like we did before) it was time for an upgrade.



    This time we ordered this Painless Wiring kit #30100 which includes a larger scale 70 amp fuse and upgraded fan relay and socket, all inside a water proof holder. That was added to the radiator support and the new fuse replaced the little Bosch relay we had in there before. The fan has worked flawlessly since. We will always over-size the relay and fuse for these high amp draw fans in the future.

    FRONT BUMPER COVER STRUCTURE ADDED + NEW HEADLIGHT

    The factory Silverado SS brackets had long been out of production, and like we did before we needed to make some more brackets to properly secure the lower bumper cover.



    I had an idea and Zach build this nice aluminum lower bracket from .080" sheet, went it up and bolted it to the frame. The bumper cover lower lip was then bolted to this bracket, and it no longer sags.



    The aftermarket headlight kit I bought in 2020 when we did the "cat eye" front end already had one "leaky" lower light on the driver's side, which failed within a couple of months of the truck coming back from paint. It was full of moisture, so when Zach was working on the lower bumper cover, he removed that light assembly. The reflective chrome film on the inside had flaked off (just this one unit), so while I looked for that replacement the guys put in a new headlight housing seal and put it back into service. Eventually I had to buy a whole new 4-piece light kit, and that one housing was replaced in January of 2023 (above right).

    WELD 20X11" WHEELS AND 315MM TIRES

    I will be the first to admit that the Fifteen15 gold 20x9" wheels were never my favorite - they were narrow, heavy, and GOLD. Even after removing the fake bolts, these wheels never looked "right" to me.



    That Fifteen52 purchase was a big compromise after finding nothing in the 20x11" size we had custom ordered in 2020 from Mobsteel (below left). I had sold my 20x9" Forgestar F14 wheels, which were a custom set that was never produced again in 6 lug in that size (below right).



    I wanted something in the 20x11" size WE KNEW would fit, but it would take some pretty exacting specs, with the same offset we made the custom Mobsteel wheel in. I didn't want to run the SUPER heavy, boring, steel Mobsteel wheels - so for a while we just kept looking.



    In 2021 Jason and I were looking at a bunch of new Weld wheels for another car and he found this 6 lug / 6 spoke version of their Ventura model line of drag wheels. It was in the same 20x11" size, then he checked the specs, and it was the exact offset we made the Mobsteel wheel in! I ordered a set THAT DAY and damned if it wasn't exactly what I wanted all along.



    Patience and persistence paid off. I like the black / machined lip look well enough, but mostly these fit exactly like the Mobsteel wheels. The 20x11" Welds were 7.4 pounds lighter than the 20x9" Fifteen52 anchors. After we test fit one bare wheel front and back I ordered some Bridgestone tires.



    I got four 315/35R20 Bridgestone Potenzas mounted and balanced with these Weld wheels in November of 2011. After checking the standard Vorshlag lug nuts we had before - the socket wouldn't fit the Weld wheels, so I got some spline drive lugs for this setup.



    It is unusual to go +2" wider wheel and +40mm wider tire and still drop 6.6 pounds in the wheel and tire assembly. The Weld wheel is more motorsports oriented, clearly. And Fifteen52 is known for "rugged" wheels that many use for off road use (hell, my Maverick just got some meaty Fifteen52 wheels for off road use). But more than the weight savings, the added WIDTH and better LOOKS is what made me go this direction.



    Wow - the change in the looks of this truck were DRAMATIC after this wheel and tire change. I started to like this truck again!



    The stance was finally right. The front bumper cover was finally fitting correctly. The tires were more flush and filled out the wheel wells. This was looking so RIGHT, but.... the continued tuning issues made me not want to drive this truck. The damn thing would die at stop lights / idle while in Drive. I got real tired of "two foot" driving this automatic transmission equipped truck really fast.

    VARIOUS TUNING ISSUES WORKED ON

    In late 2021 Zach had moved on to work at Rivian and we hired another tech that claimed to be a tuner. He diagnosed a couple of things but ultimately could not fix the issues that plagued this truck.



    We were already having trouble with the new Optima red top battery (every Optima and Odyssey battery we have purchased since ~2020 has lived a very short life - something dramatically bad happened at the factory for these two companies and we avoid these "O" brands like the plague now). The weird idle dying issue was making me nuts and at this point 4 different tuners had tried to fix it - I had receipts in the $2000 range for their various attempts to make this truck run right. Nothing worked.



    A different PCM was attempted to fix the issue. Wasn't it. A leaking fuel rail was replaced with another new truck LS unit, didn't fix the idle issues.



    We checked fuel pressure after the rail change, then swapped out the Idle Air Control unit, which was a small part of the problem. Some old, cracked wiring also showed to be faulty, so that was replaced. The issue was a LITTLE better but still required "two foot" driving to keep it from dying at lights while stopped in Drive.



    At this point it is April of 2022 and the red top was replaced with a new yellow top Optima. We tried to chase a voltage draw but there wasn't one. All Optima batteries lately just die while sitting in a car - even with a battery tender connected! We saw this happen in 5-6 other vehicles in the shop. Someone from Optima blamed the battery tender, so I bought the pricey Optima unit - same results. The red top would not come back and the yellow top still died soon after. Total junk.



    I still heard an exhaust leak and after "smoking" the exhaust one of the V-bands was then replaced. The truck still ran poorly and it drove me nuts. We're in November 2022 at this point.



    The V-band was right behind the O2 sensor so the thought was that the exhaust leak could be throwing off the tune. Some of the plugs looked a little dirty so they were replaced. DAYS were spent with my tech trying to chase down the tuning issue... still there.

    continued below
    Last edited by Fair!; 04-22-2024, 05:03 PM.

    Leave a comment:


  • Fair!
    replied
    Project update for April 22, 2024: This is a long overdue update on "TruckNorriSS" that I started writing THREE years ago, but got busy with other projects and forgot to finish. Since the last update (where I showed a tree that had fallen over a neighbor's fence and smashed some front sheet metal, then we did a 2003-07 front end upgrade), my 2000 Silverado went to my painter, came back painted, we changed wheels, did tuning, lots of other little upgrades, and then... it sat unused. So this truck is going for sale.



    Why? Hard to say why I stopped driving it, especially after we fixed all of the issues. Mostly it is because I bought a 2022 Ford Maverick, that arrived in late 2021. This was a really nice, brand new, comfortable little truck (which we added MCS coilovers to, Enkei wheels, and other mods). We also got a 2023 Bronco, a 2024 Mustang Darkhorse, and a 2024 Ford F-450. At this point I've got FOUR trucks - and this Silverado makes the least sense of the lot to keep...



    It's sad, because we finally conquered the long term tuning issues, got the bodywork and paint completed, got the rear air lift leveling system installed, and all manner of other upgrades. The truck is now finished and is going to make somebody very happy when they buy it. Right now I need to finish out this build thread to show the work we completed from 2021-2024 so I can wrap this one up. Let's dig in!

    PAINT AND BODY WORK

    I took the Silverado to our friend's at Heritage Collision Dec 23, 2020. We had already fitted the 2003-07 style front fenders, hood, lights and grill + the Silverado SS style front nose.



    They weren't super happy with the items we purchased and they likely spent more time fitting these parts than we "saved" by buying these parts ourselves. Lesson learned - listen to your painter and let them source the parts!



    They were busy and we weren't rushing them, but by early March 2021 (above) they had the panels primed, body worked, fitted, and ready for a full respray.



    By mid March they had the base and clear coats laid down and it was time to move the truck to the finish detail room (below).



    Here they installed the lights, grill, and polished the paint to perfection. By late March it was ready to pick up - I was super excited!



    This was an expensive paint job that included many days of fitting, aligning, and working all of the panels on this truck. Shiloh and his crew perfected the gaps, lined up the roll pan, and got all of the panels perfect before laying down expensive base / clear paint. I more than got my money's worth.

    FINISH WORK AT VORSHLAG

    In early April of 2021 we had the Silverado back at Vorshlag and made some time to get a few final items installed here at the shop.



    First up was this nice stainless steel replacement Chevy "bowtie" emblem, an aftermarket unit I found online. This is a meaty, CNC machined billet piece that is very well made.



    I installed this myself one day in April and it was pretty painless. The kit needed some better nuts and washers, but I managed to round up the proper hardware and got this installed with minimal fuss. The front end REALLY looks finished up now.



    The new roll pan that replaced the rear bumper needed some hardware to mount the license plate - I found a decent kit on Amazon after more searching than I thought possible. It came with GM specific hardware and included the correct square shaped, plastic threaded inserts and hardware + some foam pad material.



    Since I didn't want any extraneous branding on this truck I went without a license plate frame at first. The the foam padding was cut into squares and placed behind the plate to keep the edges from scratching the new paint. Then I used these stainless Torx style stainless bolts and special washers, which mated up with black caps that covered the hardware.



    I had purchased a back up camera license plate frame for this truck initially, but at some point I bought this carbon fiber license plate frame and installed that instead. Brad also installed this OEM black plastic cap for the trail gate. That was from a later model truck as well but with four rivnuts installed it was bolted on (there is some 3M adhesive on the top edge also). This was all done in November 2021.



    We sourced some proper 2003-07 front fender liners and I custom ordered these Silverado SS front floor mats from Lloyd's - the carpet, piping, and fit were perfect and really cleaned up the insides. #StolenValor



    Also in April 2021 I took the truck across the highway to a new alignment shop we have since used a handful of times on "non-motorsport vehicles". I had them dial in -1.6 deg of front negative camber, then checked the toe. We had the axle aligned very well so I was happy about that. The truck now drives straight, but it has an exhaust leak and still ran fairly poorly. Lots of tuning work followed over the next THREE YEARS to make this truck perfect.

    continued below

    Leave a comment:


  • Fair!
    replied
    continued from above

    GRILL & SS BUMPER COVER INSTALLED

    Mounting the SS front bumper cover happened right after the grille fiasco, sill back on Dec 15th. Zach opened the box and thankfully THAT part wasn't mangled, and it fit up well enough in the initial mock-up.



    He also started building the many sets of brackets that GM stopped making years ago. This first set of four below is for the top edge of the SS bumper cover, which always looked buckled and warped in ALL of the online videos for people doing SS front conversions. These are .080" thick aluminum with a bead rolled for strength and some bends to align, There is no template for this - it is "build to fit" time.



    You can see below how these four brackets attach to the steel bumper beam, then head up to make supports for the four taps on the plastic bumper cover. Some folks try to just attach the bumper cover with 3M tape along the top, but that is so janky - no, Zach made proper brackets.



    These brackets below became the support for the lower corners of the plastic bumper cover, and attach up to the steel bumper again



    There were other brackets along the way, including along the lower edge of the bumper cover. He also completed bolting the lower "fog light vents" to the bumper cover, but it was pretty straight forward. I did not catch every step along the way in pictures, but I do have 2 other full time jobs to cover daily, plus a lot of memes that need to be shared...



    This is where Zach got to by 12/15/20, and I was happy with the progress. After this point Brad returned from a 2 week vacation and took over, as we had Zach buried on the fab bench for weeks afterwards.



    On Dec 21st, the 2003-05 upper grille had finally arrived. Annnnd it was broken in half in a poorly packaged box. FFFFFFF!



    Being that it took a full week to arrive, and we were about to drop in between two holiday weeks, there was no chance I was going to fight with the vendor and re-order this. Time to make some repairs!



    I asked Brad to make an aluminum support for the back side and epoxy that broken part back together. There was an open channel inboard of the break, so he made the .090" thick aluminum strip, added a slight bend, and lots of scoring and scratches - to allow the epoxy to bond to the metal well. The plastic was scuffed up and cleaned as well.



    Some 2-part epoxy was mixed up and placed inside the joint between the inner and outer parts of the break, then the aluminum strip was sandwiched in there with some wooden scraps. The whole process was bonded within 5 minutes, but we let it sit overnight before putting that on the truck.



    The right front lower driving light tab also broke when it was first fitted - completely due to the cheap fenders not lining up well. Brad made another aluminum brace to fix that, with more epoxy. The next morning the headlights and grill were all installed. They actually fit, but only after a round of prying, bending, and pounding the fenders into the right angle at the headlight junctions.



    I thought this would all take about 2-3 days for the front end conversion, but it took closer to 6 - because I got a lot of cheap import sheet metal that didn't fit worth a damn, and making all of the brackets to fit the SS bumper cover was a real chore.



    PRO TIP: Much of the truck's front end has these plastic push pins and plastic rivets that hold various covers and bits in place, and being 20 years old these were all junk. I ordered this 330 piece kit for GM / Toyota / Chrysler cars for $16 from Amazon and it even came with the plastic rivet removal tool, shown. ALL of the old bits were replaced and we still have 100s of extra pins left over.

    MORE ADHESIVE REMOVAL



    This is where the truck was on Dec 22nd, with the rest of the side strips removed and soaked with WD40, trying to break down the adhesive foam that was left behind. After 20 years of being cooked by the sun this stuff was not coming off well.



    Brad fought with the removal for almost another whole day - using a heat gun, a plastic scraper, adhesive remover, the eraser wheel, and every trick in the book. He won the battle but there were a couple of chunks of paint that let go on the drivers side - we knew it was a potential outcome, but it is going to the painter.



    Wish I had done the rub strip / badge removal years earlier, but as I feared it was a lot more work than you would think.

    LOAD UP TRUCK FOR PAINT

    On December 23rd, the car in the trailer had been returned to the customer for off site storage (C5 Corvette I had driven in a couple of events in 2020) and it was time to load the truck. I have never put a truck inside this enclosed trailer, but there was over a foot of room for the roof height. No problems.



    Instead of fiddling with the winch, I drove it in, and luckily I could climb out the side window. There are some obvious hail dings visible in the rear fender above, and rock chips in every panel on the truck. Also some poorly repaired crash damage in the left rear lower corner of the truck bed. Damn near every panel needs some touch up work, so we're going with a full respray. I thought about a color change but that entails jams, bed removal, underhood painting - more time and money.



    I had purchased a 2003-05 OEM Silverado rear tailgate cover (it has a slight "spoiler shape" to it), but when Zach pulled the 2000 plastic cover off it was obvious this was a 2003-05 tailgate - the factory installed nutserts for the later tailgate cap were hidden under that. So that install just got easier.

    CHANGES AFTER ARRIVING AT PAINTER

    On Dec 24th, I dropped the Truck at Heritage Collision Center in Sherman, TX. And picked up a customer car we had there getting body work done...



    The owner there (Shiloh) has painted countless cars for us, and know my tastes. He asked me - what about the chrome rear bumper? The likelihood of towing with this truck with a C-notched frame is ZERO, so he told me to buy a bolt-on roll pan. This way we can ditch the last of the chrome - the rear bumper - as well as the tow hitch, heavy spare tire, and really clean it up back there.



    He told me to get a bolt-on instead of a weld-on or fiberglass roll pan, so I found one with an LED license plate light on Amazon - after checking way too many sources. I also bought a pair of power side mirrors from DNA Motoring, again, who I have bought many things from before.



    After being slammed into from behind while stopped in traffic in my 1999 GMC truck, I am a bit paranoid about having BRIGHT brake lights. So one of the first upgrades on this truck was an aftermarket LED 3rd brake light, shown above left. This was installed in August 2017 and worked great, but it has yellowed BADLY after 3 years of being parked outside since, so I ordered a new one - that is smoked. I stewed over this choice and might ditch it if it looks out of place, but at $35, who cares, right?

    WHAT'S NEXT?

    Almost all of the front end was thrown out, except the headlights (which I gave away to someone that works at HPR) and these 2000 Silverado front fenders. They are probably worth something to somebody, but no, they won't be worth shipping. The RF fender has a dent that could be repaired and the LF is in excellent shape - and they are OEM parts, so they actually fit.



    The new side mirrors, updated hood bumpers, and new LED 3rd bake light have arrived, and all we lack is the rear roll pan. It shows to arrive next week, and I'm taking another race car to Shiloh's shop for bodywork and paint around then - so I can take all of the truck bits with me on that trip. Can't wait to get this truck back, get the exhaust leak fixed, install the air compressor for the rear helper bags, and GET THE FINAL tune dialed in. I am also going to have the Fifteen52 wheels repainted a bright color. Stay tuned for that, soon!

    Thanks, and have a Happy 2021!

    Leave a comment:


  • Fair!
    replied
    Project update for January 1st, 2021: "New year, New me!" Trying to catch up on many of our forum build thread updates on the first day of 2021 - and the shop truck should be an "easy" update. Over the month of December a chunk of work has been done on the Silverado. It sat behind the shop (below) for a few months longer than I had hoped, before we could get to it.



    We were as busy as ever in the shop, trying to get some work done on customer and shop cars. We had a bit of luck and hired a new fabricator / mechanic / engineer in October, Zach, and he did a big chunk of work on the truck since then. Brad took over when Zach got buried with production fab work and brought all of the front end work to completion.



    The tree that fell onto the truck in a windstorm in August 2020 did some real damage to the roof, RF fender, hood, and popped out one of the headlights. What Zach and Brad accomplished in about two weeks of work was to remove the 1999-2002 front sheet metal and replace it with a 2003-05 Silverado SS front end.



    I also learned some valuable lessons about the GMT800 and the Silverado SS model - replacing bad information I had learned elsewhere. Like many mistakes it cost me time and money - so if you want to learn from my mistakes, read on below. That's the whole point of these posts, after all.

    SOURCING THE PARTS

    There were a number of other little dents and dings in the truck that I wanted to have repaired. I wasn't looking for a show car but 20 years had taken its toll on this work truck and it was time to implement some modifications I have wanted to do on all 3 of the GMT800 generation GM trucks I have owned. I showed pictures of the Silverado SS in my last post, and I will share more information about this short lived SS model in a section below. First up, I needed to order the 2003-05 front sheet metal as well as the Silverado SS specific bits.



    Having owned three of these GMT800 trucks (1999 GMC Sierra 1500, 2001 Chevy Silverado 1500HD, and this 2000 Silverado 1500) I knew surprisingly little about the sheet metal on the "post face lift" trucks, which happened in 2003 and ran all the way to the 2007 model year. I knew enough to order 2003-05 Silverado 1500 front fenders, hood, front bumper mounts, front bumper, headlight mounts, and headlights. I got all of the sheet metal, grill, and SS bumper cover from the same manufacturer through Summit Racing (Atech) and most of the rest I found on eBay. All of this was fairly cheap import replacement parts, which would come back to haunt me later.



    I've used this "DNA Motoring" brand of headlights ad parts many times before and they worked out well, including the 2000 model aftermarket headlights I bought for this truck in 2017 (which still look perfect). Of course this is import stuff, but almost all of the headlights are anymore. I liked the slightly non-OEM look of this version above with a back trim ring but clear (not smoked) lens covers. Sadly I spent far too long looking at the MANY non-stock headlight versions.


    Much of the OEM front end parts for mounting the Silverado SS bumper cover are no longer available, and the handful of GM sourced bits that are available were ludicrously expensive, so I knew we would have to make a lot of these hidden bits. Not to worry - we have fabricators.



    Of the many external appearance items on the Silverado SS, I wasn't too keen on the lower body cladding, shown above. It was hard to source, expensive, and a bit too chunky for my tastes.



    I might change my mind later on and add that, but for now it will be left off. I have seen many "conversions" done where this was deleted (above left). It only stands out if you look at them side by side...



    Almost all of the "Sherman" branded sheet metal, front bumper, bumper cover, and grill parts arrived from the manufacturer on a pallet on Sept 2nd, with a $100 flat shipping charge. I used the tractor and forks to get that load from a big box truck down the road. The hood was back ordered and showed to be delayed until at least December, and that looked like it would ruin my "rushed" repair timeline (ha!) so I cancelled that hood and got another from another brand, also through Summit. Had to pay another $100 to ship that, which sucked, but it arrived soon after.

    FRONT END SHEET METAL FITTING

    Months had passed since the tree fell, and we had caught up on several customer jobs and had a lift free for maybe 3 days. Perfect! On December 11th, 2020, I charged up the battery and drove the truck in front of the shop for a good wash. Sitting under trees for months left a lot of sap and leaves, but it all cleaned off.



    After bringing the truck into the shop, one of the first tasks is to remove the front headlights, grill, and front bumper. Then we laid out all of the 2003-07 bumper support and headlight bucket parts I had purchased months earlier.



    After removing the front fenders, Zach then looked up the videos I had sent him to learn what to cut and where. The 1999-02 bumper supports are cut off flush at the frame rail.



    Various tools were used to cut off these bits - SawsAll, Spinny Wheel of Death on the die grinder, angle grinders, and more.



    Lots of sparks and ... success. The remains of the old front bumper supports were swept up, along with a few dead saw blades, and dumped into the trash.



    Before I could blink he had the new 2003-07 front bumper brackets welded on with the MIG and primed. These can be bolted on, as they are meant to be a retrofit mount, but again - we have fabricators so we do it the right way.



    The bumper brackets were installed on the same Friday (12/11/20) that I brought the truck into the shop. Zach started installing the new 2003+ fenders as well.



    There isn't any real inner fender structure on a full frame vehicle like this, as the front fender has the inner structure welded into it. So with the front fenders out the aluminum front radiator support structure can flop around like a dead fish. To access some of the mounting bolts things like the battery and fuse box have to be shoved out of the way. A bit time consuming, especially when you have to go back and remove a fender to adjust something.



    The hood went on, but we could tell right away that there was a dent in one corner from shipping, and it didn't fit well to the front fenders. The old headlight bucket mounts came off and went into the trash, then it was time for the new buckets and the new front bumper.



    When I ordered the 2003-05 steel front bumper I opted for a black painted one instead of chrome. I hate chrome, and it costs more, and would be hidden under the SS bumper cover anyway. Pretty quickly after Zach mounted the bumper, the upper headlights and grill were in! One of the lower headlights wasn't fitting well and I was "helping" when one of the tabs broke. The fenders were not aligned to the nose well, and made the lights not fit.

    Still, I was happy with how this looked after only 2 days. I was "smart" and ordered a later 2006-07 "Intimidator" SS grill, which has a hexagonal pattern that I thought looked better than the earlier ones. I was able to locate a similar set for the lower grill opening on the SS bumper cover, but had not found the "fog light vents". Yet. So we closed the hood and...



    FFFFFFFFFFFFFFFFFFFFFFF!!!!!!!!!!!!

    CHANGES ON THE SILVERADO SS MODEL RUN

    Much of what I knew about the Silverado SS I learned from this very short wiki entry:

    Chevrolet Silverado SS

    Launched in early 2003, the Silverado SS is a high-performance pickup truck built by Chevrolet. It is based on the 1500 Silverado Extended Cab with Fleetside Box and features upgrades in the drive train and both exterior and interior appearance. It was equipped standard with the 6.0 liter Vortec High-Output V8 rated at 345 hp at 5200 rpm and 380 lb⋅ft of torque at 4000 rpm coupled to a 4L65E four-speed automatic transmission.

    The SS debuted in 2003 with a standard All Wheel Drive setup with a 4.10 final drive gear ratio and 4 wheel disc brakes. In 2005, in an attempt to increase sales, a 2-wheel drive version became available (the 2WD SS also lost its rear disc brakes in favor of drums, as did the rest of the 1/2-ton GMT800s). 2005 was also the first year the sunroof was available in the SS line up. In 2006, the AWD variant was dropped and the rear wheel drive was the only driveline layout available. In a further effort to reduce cost, buyers could also choose cloth interior and/or a bench seat. The Silverado SS also comes with the Z60 performance suspension and 20 inch aluminum wheels. All the SS trucks in both 2 wheel drive and AWD used the torsion bar style front suspension for better handling. SS themed trucks were only available from the factory in Black Onyx, Victory Red, and Arrival Blue Metallic from 2003 to 2004. In 2005 Arrival Blue Metallic was dropped from the color choices and replaced with Silver Birch Metallic.

    Intimidator SS

    In 2006, Chevrolet released a special edition Silverado SS under the name "Intimidator SS" (licensed by Dale Earnhardt, Inc.) to honor the late Dale Earnhardt. The truck came with several minor appearance upgrades (rear spoiler, embroidered headrests, Intimidator custom badging), but was essentially a standard Silverado SS. Of the 1,033 scheduled trucks, only 933 were made (the remaining 100 were sold as 2007 Silverado SS "classic" body style trucks before the 2007.5 MY changeover. These trucks were only available in Black Onyx exterior but could be ordered with cloth or leather interior.




    What this wiki (and my lack of knowledge) failed to point out was that the 2003-05 model SS (above left) had the same flat hood as I had purchased, but the 2006-07 model SS (above right) used the TALLER HOOD from the 2500HD/3500HD hood. Which has a raised front section and a completely different grill shape, along the top. It is hard to tell even looking at them side by side now... but my ignorance caught me out with the wrong grill choice.



    Most of the "Silverado SS" models I had been looking at online were clones anyway, short cab versions, most lowered, and many with hideous aftermarket hoods. I never liked the "tall" hood on the HD models so it never occurred to me that GM did this update to all SS models in 2006. This is where I learned another lesson and had to re-order some parts

    ORDER CORRECT & MISSING PARTS

    So after diving into a bunch of really weird forums devoted to trucks (there are a LOT of these) I found the error of my ways. But sourcing the correct upper grille on December 15th was going to be tricky, with the complete train wreck that is the "holiday shipping rush". None of my usual suppliers had ANYTHING remotely correct for the OEM 2003-05 SS grill I wanted. There were several different "shapes" of the diamonds offered by GM for the upper grill, lower grill, and "fog light vents" - and crazy me, I wanted them to match.



    Jason found this unusual supplier "topgear autosport" above left, who had the correct year and diamond shaped upper. It was not marketed as an SS grille but it looked to have the correct upper shape, and they said they had it in stock online. I also ordered the correct 2003-05 hood bumper rubbers, which lines up where the fender meets the hood (these took weeks to arrive) via eBay. I also ordered the same diamond pattern 2003-05 lower grill insert for the SS front end, also from eBay. Paid more than I wanted to for all 3 items but I needed them before the truck went to the painter.

    continued below

    Leave a comment:


  • Fair!
    replied
    continued from above

    COOLANT TEMP ISSUE

    June 24th was a very hot day here in Texas and I was using this truck to driving all over town, making deliveries and pick ups of parts with vendors. I had the AC on high and was parked for a minute waiting for a vendor, then loaded up, and as I was leaving - SPLOOGE! Dumped a bunch of coolant as the radiator cap popped. This overtemp issue lasted only seconds before I shut off the engine and pulled over.



    I let everything cool down for 15 minutes then limped back to the shop to refill the coolant (water + maybe 20% coolant) in the aluminum radiator. What happened?



    Turns out the relay powering the electric fan burned out, so the fan wasn't coming on. This wasn't an issue driving above 40 mph, but below that and at idle, with the AC on full blast and with 98°F summer heat, it was too much. We've replaced the relay but will likely upgrade to a higher amperage unit, or a solid state relay, to prevent this from happening in the future.

    DE-BOLTING THE WHEELS

    In early June 2020 I couldn't look at these silly wheels any longer. After fruitless searches on what these bolts do I just decided to remove one and see... sure enough, it was fake. Did nothing, didn't seal anything, just a blind hole in the heavy cast wheel. I took 100+ bolts out of the 4 wheels and they totaled 1.7 pounds.




    Maybe 20 minutes to get all of these off, pick up all of the bolts, and nothing else was needed. My only regret was not doing this THE DAY these wheels were mounted. Big improvement in looks, and if the black band was all the same color it would look better still.



    This is the current ride height, above, with the rear bags lifted just a hair for a slight rake. This way I can pick up heavy loads of parts and never worry about bottoming the rear suspension. The truck stayed like this for a few months until 2020 struck.

    IF A TREE FALLS IN THE WOODS...

    2020 has been a rat bastard of a year! We had a big storm blow through on August 16th and, while we never heard the crash, a tree fell onto the roof, windshield, hood, and front fender of the truck, doing some real damage.



    This tree was long dead, and on our neighbor's commercial property. Texas case law is pretty clear on trees, it's a natural event and nobody is liable. But when the tree was dead for years it can be considered neglect, and the owner owner property where the tree was might be liable. It's a big mess is what it is.



    I took the video below the morning after this happened. The damage was pretty obvious - roof caved in, windshield busted, hood, fender, even popped a driving light out. This is not what I needed, but hey - its 2020.



    I went and talked to the neighbor, who quickly sent a tree crew to come by and chainsaw the tree into smaller chunks and haul it all away. I used the tractor to lift the tree off the roof, then drove it to a car wash to get all of the busted limbs and twigs out of the bed and clear off the exterior to see how bad it was.



    With the paint cleared off the damage was apparent. Roof skin is toast and the dents in the hood are enough to warrant replacement, ditto the fender. I had a friend do an estimate but at $5600 is is a bit daunting, and I don't think anyone will foot the bill for this. It's gonna be on my dime, more than likely. So if I am going to cover the costs, it will be time for an upgrade....

    SILVERADO SS CONVERSION DURING BODY REPAIRS



    Looks like now is as good of a time as any to turn my 2000 Silverado into a Silverado SS clone. This was a specialty truck Chevrolet built from 2003-2006. Yes, it is a total cliche, and yes, I am that basic.



    I have to replace the hood, a headlight, and fender anyway, plus the front chrome bumper had a big dent in it (some a-hole backed into me in a parking lot) and the original grill was already busted. So I might as well get the hardware to convert to the 2003-07 front end: fenders, hood, headlights, grill, headlight mounts, bumper, and bumper brackets. Then it isn't too far of a jump to the SS front end, which is a unique set of grills and a lower bumper cover. I've read up on this for several years, as it was always part of the long term upgrades for this truck.



    I thought briefly about a color change but that is REALLY hard to do well without a LOT of extra spending - so it will stay white. And I will include a white rear bumper. Within 5 days of the "tree incident" I had already researched and ordered all of the body panels, bumper, brackets, headlights, and grill. Most of the shipment is here or inbound, all except the hood - which is 2 months out. Damn pandemic!

    MISC REPAIRS

    When the truck was on the lift recently we noticed the pinion seal is leaking, as are the "slip joint" connections for the ARH exhaust aft of the headers. We will tackle those repairs with the bed is removed, which needs to happen during the Air Lift compressor / controller install.



    Right now that is the least of my worries, heh.

    DE-BADGE AND REMOVE RUB STRIPS

    On August 19th, two days after the tree incident and right after washing the truck, I decided to get off my butt and start on the de-badging and rub strip removal. I had meant to do this 2 years earlier, and now if I screwed up the paint removing these plastics I can at least have the paint repaired during the impending paint and body work.



    I left the truck sitting in the hot sun for hours and broke out a few tools: some plastic wedges, a hunk of heavy string, and an eraser wheel on a drill. The badges were easy to get off just with the wedge.



    For the side rub strips, these were ON THERE good. I started them with the wedge, then slipped a hunk of string underneath and "sawed" through the adhesive foam. At a certain point I just started pulling the rub strip off. This left a LOT of gummy foam adhesive in place.



    Then using a $20 eraser wheel on a drill I was able to "Erase" the adhesive foam. It wasn't easy but it wasn't harmful to the paint or clear coat, luckily. I ran out of steam about an hour in (it was hot as hell outside) and soaked the rest with WD-40 - which will help loosen the adhesion for additional work in the near future. It already looked good only half done on one side, above right.

    WHAT NEXT?

    I will chronicle the 2003 / Silverado SS conversion, showing all of the custom bits we will have to make (GM doesn't support vehicles after 10 years so many of the SS parts are no longer available). I will likely have the wheels refinished in one color while the truck is at the painter (on the 17" wheels/tires), too. Lots to do!

    Cheers,

    Terry @ Vorshlag

    Leave a comment:


  • Fair!
    replied
    Project update for Sept 1st, 2020: Five months have passed since our last forum build thread update on the GMT800, and a number of items we were waiting on have arrived, been installed, tweaked, and tested on this 2000 Silverado. Changes to the tune, rear "helper" air bags fixed a ride height issue, new wheels and tires we added, we did follow-up 0-60 testing, and more. We had the truck looking better than ever (below left), then the worst it has ever been (below right)...



    Yes, it is 2020 after all, so of course a freagin TREE fell during a summer storm and caved in the roof and did some other damage. I will discuss that and the new upgrades happening during this paint and body repair.

    RETUNE + 0-60 TESTING

    Let's back up to April 2020. We had been struggling with the tuning on this new engine setup for 6 months, trying to get the custom dyno tune and driveability "right". One shop tried 3 times, two other tuners both took a crack at it, but there was always still some serious funkiness going on in daily driving. After the engine swap I only ever used 93 octane fuel, which was in the tank at the very first tuning attempts.



    After changing the main ECM, then O2 sensors, TPS sensor, MAP sensor, spark plugs and more attempts it still would not idle in "drive", stopped, with your foot on the brake. And on top of that the part throttle shift points were all whacked. I spent 6 months and a good deal of money chasing these phantom tuning and driving issues, which was a bit frustrating.



    Jon Simpson of JS Performance has fixed some really screwed up race car tunes for us, and regularly tunes 500-3000 horsepower engines. One day he was in town and brought his laptop to the shop, then spent about 45 minutes on this truck - and found the issue. There was some lingering OEM torque management issues that were making the engine want to die just idling, and he got rid of that once he found the issue. He also raised the idle rpm, and did some driveability tweaks, but was on a tight time budget and that was all he had time to tackle. We still need to re-tune this on a dyno, and the next time he is in town I'll pay him to do that and tackle some of the driveability changes.



    After it was running right, finally, it was time to test the 0-60 mph sprint with the big changes we wrapped up in early 2020. Later that day I went down to Mexico and tried several times to get a good "after" test. This was with the new 5.7L LS engine, ARH headers, new quiet exhaust with the massive Magnaflow muffler, 3.73 gears, the mini "stall" convertor, built 4L60E trans, and Dorman intake. This testing was done on the stock 17x7" wheels and relatively hard 265mm tires. I have power plans beyond this level of mods and wanted to get an interim acceleration test in.



    Here are the Before (left) and After (right) videos of the 0-60 mph tests, on the same road, in similar weather, and on the same tires. Before was right before we did the engine swap at 8.80 sec, after with the new setup was 5.91 sec. A 3 second gain is nothing to sneeze at but we've still got some room to improve.You can never have "too much" power, ya know?



    The "After" test was still a bit frustrating, as you can see in the video. The "higher stall" convertor turned out to be more hype than help, as it feels like a dead stock convertor. Doesn't stall ANY higher than stock and the shifts on the built 4L60E are too firm and we need to work on some of that in the tune. The shift points at WOT are great at 6500 rpm, but in low throttle normal driving are less than ideal. Having a tuner 5 hours away makes this difficult to tweak, but we'll have Jon here soon enough to tweak this.

    All in all a 3 second drop for 0-60 mph is plenty good, and that was traction limited. We need to test this again after the next re-tune and with the newer tires, shown below.

    FIFTEEN52 WHEELS AND 275MM TIRES ADDED

    I have said this many times: "Wheels make the build." And it is no secret that I've been having a helluva time finding the right wheels for this truck. I want them wide and light, but also strong for street use with a livable daily driver tire. As I have posted before, we did manage to fit a custom 20x11" wheel and 315/35/20 tire under the stock fenders, and they don't even look that "big" when you see them on the truck.



    We made this test wheel based on our measurements using Mobsteel - and have since have searched the world over for something in this size and backspace in aluminum, to hopefully avoid using these BOAT ANCHOR wheels: 53.2 pounds for the bare wheel and 87.0 for wheel and tire is obscene!



    Jason and I must have looked at 400+ wheel companies and models. The 6 lug is the killer - almost nobody makes this bolt pattern in anything wider than 9" that doesn't poke out the fenders like a roofer's Brodozer wheel. Custom wheels made to our specs in this bolt pattern and offset were going to run $1700. PER WHEEL. The light and wide custom options just sucked.



    We have access to many wheel brands through a wholesale account and Fifteen52 was one we can resell. We had even called these guys back in 2019 about getting this custom 20x11" wheel made, since they already made a 6-lug wheel. But they pretty much blew us off (with the minimum order and pricing), and their cast wheel weight was less than ideal. Then Fifteen52 and our wholesaler they had a sale on these, and I got this set for a ridiculously low price - in a weird color scheme of gold and black, with these ridiculous bolts. I bought them so well that this was a fairly low risk purchase. I just HAD to get the stock 17x7" wheels off this truck!



    Yea, it is heavy at 37.6 pounds for the wheel and 72.1 pounds for the wheel and tire. And the wheel looks a bit "Busy" in person, with the two colors and the damned fake bead lock bolts. At only 9" wide wheel and a 275mm tire, it seems a bit small. When it comes to tires, if it doesn't start with a "3" it doesn't belong to me...



    Compared to the same 20x9" sized Forgestar 6-lug F14 wheel (25.6 pounds) we had on Truck Norris (and which I foolishly sold - and they won't make again unless I order 100+ wheels) these are a bit uglier and heavier.



    Tire choice was possibly a bit rushed - this wheel sale popped up in a size I wasn't really looking at and I mistakenly ordered a 275/45/20 tire, meaning to order a 50 series for a bit more sidewall. A taller sidewall means a better ride and the ride quality with these definitely suffered. I went narrow because the calculations we did on this 20x9" setup showed that the outside edge was going to be TIGHT with the fenders. A 285/55/20 might have looked better bit it might have rubbed, too...



    This is where the truck sat on 5/21/20, after installing these wheels and tires. The gold isn't really my thing, and the Ken Block style is a bit much with the bolts. These shorter tires definitely amplified the reverse rake we have going on here, too. And the rear can bottom out (axle to frame mounted bump stops) with it this low in the back. Time to fix that...

    REAR HELPER BAGS ADDED

    Well the next day (5/22/20) the Air Lift "Slam Air" rear air bag kit I had ordered in February finally arrived. The pandemic really killed delivery times for a lot of companies, and even waiting 3 months we still weren't showing to receive the matching compressor and controller for months more.



    Ever since we started the "3/5" inch front and rear Belltech drop kit, we have had ride height problems. The front and rear each dropped closer to 7 inches with their mislabeled kit, and we "fixed" the front with the spring spacer. But the rear was now still too low (reverse rake) and it is not as easy as you'd think...



    And with the axle flip (below left) you get a BIG chunk of rear ride height drop that you cannot easily claw back. Seven inches using the stock rear leafs and shackles. On an old school leaf spring rear suspension we'd just change to a longer shackle to raise the rear. But this truck uses a reverse shackle on the rear, as shown below right. We would have to use a SHORTER shackle to raise the rear. And since the shackle is located at one end of the leaf, any changes here will only make for HALF that in ride height. My 1999 GMC had an aftermarket longer shackle to lower ride height, but with the poly bushings most come equipped with it would "stick" when the shackle articulated... and POP back down under braking. The aftermarket solutions for shackles for this truck just plain sucked.



    We brought the truck in onto the lift and I had engineer Myles and technician Evan look at this with me. The "right" way to fix this would be to cut off the rear shackle mount and lower it relative to the frame. Or just make a new bracket altogether. This turned out to not be a "small task" and instead of wasting engineering and shop hours making these one-off brackets to raise the rear about 1.5 inches, I decided to just "do it with the bags".



    At this point we had the truck in the shop and the Air Lift bag kit was here, so I juggled our schedule a bit to go ahead and install the rear bags, to raise the rear ride height and hopefully make this truck more driveable again. Ever since we lowered the ride height I have been fighting this thing and not driving it much. The shorter sidewall tires only amplified those issues.



    We took the time with the truck on the lift to properly center the axle, side to side. When we had performed the axle flip and C-notch work we were on a time crunch, and the axle alignment wasn't properly setup. With the narrower 7" wide stock wheels it wasn't a bit deal, but with the +2" wider 20x9's on the back it was clear we had about a 1/2" offset on the axle. The pic above right shows how "inset" that tire is - the opposite side almost poked. We cleared that up that day; re-centering the axle made for better tire clearance in the back, as these wheels are pushed ALL the way out to the edge. The added with on our 20x11" wheel is all inboard from here.



    Above left shows the clearance to the (modified) ball joint stud with the Belltech drop spindle and ball joint on the 17x7" stock wheels. I took a shot (above right) with the truck on the lift to show the new 20x9" wheel, and the added clearance is apparent. Now we can add stock replacement ball joints and not have to chop the stud and nut off to clear the 17" wheels. But once we do that... I'm stuck with these wheels and tires as my only option, as the 17" wheels would not longer clear the full length ball joint. Instead of installing the new ball joints I punted - going to wait until I paint these wheels a different color before I limit my choices.



    This kit was supposed to be 100% bolt on, but of course since we have a C-notch kit on this one the bolt holes are all covered up. We tossed around a few ideas and settled on "let's cut and weld" to fix it. So the bags go on the axle exactly where the Air Lift kit instructions show, and set ride height and added the bracket to allow for some expansion / lift with some air. We needed to raise the rear about 1.5", so inflated that's where we want to end up with the bags.



    Evan did the surgery and welding, then primed and painted the whole area with gloss black paint. Routed are lines from both bags to a regular Schrader valve by the rear license plate. Now we can raise or lower the rear with an air chuck - at least until the compressor / controller kit from Air Lift arrives.



    This pic shows the "leveled" ride height we started with, which I have since raised up another 1/2" or so. I've been driving the truck for almost 4 months like this, waiting for the time to install the compressor / leveling controller, after it arrived 2 months ago. The ride is definitely FIRMER now with the inflated bags, but the axle never once has touched the rear bump stop.

    I have since hauled all sorts of loads in the bed of this truck, including 500+ pounds of steel parts more than once. No issues whatsoever with hauling stuff now, at least. Wish it rode a little better, but we'll look at this next. This was my walk-around video from the day we installed the bags.

    continued below

    Leave a comment:


  • Fair!
    replied
    continued from above

    This weird issue persisted and we chased this for weeks. Evan worked on the tune, Anthony from HPR looked at it, Jon Simpson from JS Performance tweaked on the tune. It was maddening! The only thing that made sense was a bad ECM or some funky "base programming" in the old ECM.



    So Evan swapped in the ECM from my 99 GMC, then copied over the TSM tune in chunks. It seemed to make it better for a little while, then it started re-learning bad habits again. It needed to go back to the dyno, with some other changes, for more testing.

    EXHAUST SYSTEM UPGRADE

    One of the changes that I wanted done before the truck went back for a THIRD dyno tune was a QUIETER exhaust. This twin 3" system was not TOO loud on the 99 GMC with the same long tube headers on a stock 5.3L, but with the built 347" and big came, and dumps - it was deafening.



    We went back to a known quiet / high flowing muffler - the Magnaflow 12589. This is their LARGEST 5x11" oval muffler case at a staggering 22" long and 18.5 pounds. I had actually bought TWO but we couldn't fit both under the bed.



    Not only did I want to run TWO of these I also wanted the exhaust to go over the axle and out the back. Not going to happen without major surgery under this truck. The axle gets too close to the bed and the over-the-axle routing is nearly impossible. Getting a tip going out the side in front of the tire wasn't an option either - this muffler was just too big. But it NEEDS to be big to kill the exhaust noise...



    Everything is a compromise and in this case I listened to Evan. He mocked up a single muffler then made a custom 2-into-1 merge using some stainless bends we had on hand.



    Evan made the merge and joined the front 3" dual exhaust into the muffler. Looked good but I was worried it would be too loud.





    He mounted it up (above left) and said "let's test this" before we try to make a tortured over-the-axle routing or something else. It sounded QUIET and GOOD. Amazing. OK, that will work, just add a little turn-down and we will go with it.



    So this shot shows the full exhaust with the ARH Long Tube headers, cats, our 2-into-1 merge and the Magnaflow muffler with a turn down. This was relatively easy, packages well, and sounds REALLY good. Quiet as a church mouse driving at normal RPM but you can here it when you are doing pulls up to 7000 rpm!

    LED DLR & TURN SIGNAL BULBS, SOCKET

    So I am not one to complain about Daylight Running Lights, which is required in some countries on most cars. This truck had that feature but one of the lights has been burned out since I bought this truck. This is a COMMON ISSUE on the GMT800 trucks and SUVs - likely 75% of these still on the road heve ONE bulb out on their DLR system.



    What happens is the socket burns up (see below left) - but there is a cheap solution. This new socket with pigtails (below right) was an easy fix.



    Brad had that wired in to replace the old socket in no time. Should have done this years ago, but we had some time and now we could install new LED bulbs in all of these sockets (below left).



    I bought these LED bulbs online years ago also, and they went in fine. Wow, much brighter parking, turn, and DLR bulbs! I think these were 5000 K color, so the new LEDs look a lot different than the old, Halogen bulbs in the headlights. I'll tackle that next.



    But the turn signals had a "fast blink" issue, which is a common problem. Brad installed some a resistor kit on the turn signal circuit that I had, but that didn't work. Removed that and installed this "Fast blink" flasher unit, from Diode Dynamics. Also not fixed. Hmm, I will call DD and see what they suggest next and circle back around to this in the next update.

    REAR SUSPENSION MODS - ROUND 2

    The stock length Bilstein 4600 dampers only lasted a few days of driving - needed to put some miles on the truck for testing of the tuning attempts but the rears were bottoming out. One shock blew out and that side dropped 1/2", due to the loss of gas charge. We immediately started looking at shorter shock options from Bilstein.



    Jason poured through the catalogs, did some math, and came up with 4.75" shorter damper with the same total 7.5" of stroke. This is possible due to the remote reservoirs that come on this particular option.



    This 8165 series monotube Bilsteins was the answer. There were crap pictures online so I shot these in the photo booth. These came with two reservoir mounts per shock, the band clamps, and looked really nice.



    Normally we mount remote reservoirs on the chassis away from the shock or other heat sources, but the hoses were pretty short and the included polyurethane mounting blocks were pretty nice - so I asked Brad to just mount them to the bodies. I wouldn't do this on a road race car or off road racer, but for the daily driver it works more than fine.



    These are made for another vehicle, of course, and had 1/2" holes in the included steel sleeves that slide into the poly bushings at both ends. Evan drilled these on the lathe for the stock 14mm bolts (with a 14.1mm drill we have) and Brad pressed those into all four shock bushings. Not much work to have this custom shock setup.



    Included in the Belltech kit were these bolt-on rear shock mount extensions, which Brad noticed were already loose - they could pivot slightly. Nope, that's not gonna do. Evan welded them to the axle housing and that firmed up the lower mounts.



    After installing these the ride height was back up that 1/2" on the one side where the OEM length Bilstein 4600 had blown out. Once that was buttoned up it was time for a test drive across town and back, doing some "parts hauling" chores this truck used to do again. The ride quality was PERFECTION - front works great, now the rear could soak up bumps and had LOTS of suspension travel. This was hopefully the last tweak needed for a bit.



    This is ALMOST right. The rear ride height is still a tick lower than I like, and the factory leaf spring rates are a bit too soft for hauling parts or towing, so we ordered some helper air bags that I can bump up as needed. This included an Air Lift branded "Slamair Kit" and "Load Controller Dual Heavy Duty Compressor". This has air bags / mounts for the rear suspension that I can air up at the touch of a button to raise the rear ride height when needed. I will show this next time - the parts are on backorder.

    3.73 REAR GEAR + AUBURN LSD UPGRADE

    This truck came with 3.08 final drive ratio in the axle and it was an "Open" diff. It was time for a gear change and a limited slip + new bearings & seals throughout. Been wanting to do this for years and finally have an excuse - the extra power from this 347" engine has turned this truck into a "one tire fryer!" and the tall gearing prevents a safe 3rd gear dyno pull.



    This was a BIG change but one I decided to do before Round 3 of tuning, which should happen later in March 2020. Jason ran the numbers for me and gave me several options for final drive ratios with the stock tires + the 315/30/20s I wanted to run in the future. The chart is below...



    The top speed in 3rd gear before was 182 mph with the stock 3,08 gears - no wonder they didn't dyno in that gear, ha! I decided to go with the 3.73 rear ratio as the best compromise. Everything is a compromise - this will keep 80 mph cruising speeds at only 2500 rpm (in Texas we have some 85 mph roads) while waking up the acceleration in lower gears.



    This engine is just about doubling the power output of the 4.8L it had before, which has led to severe traction issues. While doing the gearing it was time to send power to both rear wheels. We looked at a Torsen style True Trac but I could not rule out the Auburn Pro limited slip unit - which worked very well in our 2018 GT. Price was better, too. And we've have great success with Moser parts on other projects, so that skanky old stamped steel diff cover will be replaced with this meaty, cast aluminum Moser cover. It has a drain and fill plug and includes bearing pre-load studs. It also looks damned good.



    On March 12th we had scheduled for Donnie to stop by and do the install. He has done our gear installs for the last 8 or 9 years and every one has turned out perfect. This is a specialty job that you get better at over time - so we bring in this "gunslinger" for diff and gear installs.



    Donnie popped the rear cover and we realize that the spare tire needed to be removed - should have had that out of his way before he got here. We inspected the magnet on the back cover, which was covered in "fuzz" from wearing gears and such. Time to remove all the guts and clean out the housing.



    Rear brakes removed, axles pulled out, then the center section and pinion. We were replacing all of that so it was scrap metal. Donnie cleaned the inside of the housing out and got to work on the seals and bearings.



    The axle bearings looked pretty toasty so we ordered new bearings and seals from a local parts house. Donnie installed those both and got to work on the new center section.



    The new 3.73 ring gear went onto the Auburn housing and the new pinion went in with a setup bearing. After a few iterations with shims and gear paint he had the wear pattern spot on. Then he set the back lash with the new diff housing side bearings.



    Then it was time to put in the new pinion bearing and seal to button it all up. The new Moser cover went on with some gasket maker and the diff housing was filled with Motul Gear 300. The bottle of friction modifier from Auburn went in and it was time to put the truck through the gears up on the lift. Dead silent. then the spare tire went back up in place.

    While he was here Donnie took a crack at the tune, using our laptop and HP Tuner cable. He noted some weird stuff going on - one O2 was cycling the other was "stuck". The timing at idle was a mess so he locked in the minimum idle timing at 13 degrees advance. A few tweaks with the IAC and it was idling better. He noted that it still "had problems" but in his brief test drive he said it was driving nicely. Donnie was all wrapped up with the gears and tuning tweak before lunch, and we had some test drives to make.



    Evan and I drove the truck to lunch and back that day. Holy cow, it drove SO WELL on both drives! Idle was perfect, acceleration was strong, manners were spot on. Whatever Donnie did worked like a charm. Did a first gear rolling acceleration test on some dry pavement in Mexico - both rear tires lit up as it pulled hard to 7000 rpm, shifted firmly into 2nd, just pulling hard through the gears like a beast. Normal driving was tame, quiet, perfect. THIS IS WHAT WE WANT! All the time.

    PROBLEMS RETURN - THE FUN WITH TUNING?

    Drove the truck again just a few hours later that same night, a few miles into town to dinner and back, and it was a COMPLETE MESS. Something happened again, after just two short drive cycles. It was dropping 4 cylinders every 5 seconds, lost 80% of the power it had at lunch, wouldn't idle, just JUNK. Dirve cycle number 3 once again.



    This is getting ridiculous. It was time to start changing parts out. Evan pulled the plugs and they looked like crap, black from running pig rich, after less than 100 miles.



    Evan swapped in a new set of NGK TR6 plugs, which should work fine for this engine with 93 octane. A little hotter than some engines we have (we tend to use TR7 or TR8 on race engines) but this is my daily driver. We ordered the front or "primary" Oxygen sensors for both banks as well as a new Throttle Position Sensor.



    One of the tricks Jon Simpson suggested was slotting the TPS to get it to idle in the right voltage range, which Evan did with the new unit. He wrapped up this round of parts installation and... still ran terribly. It needs to be loaded up on a a dyno and tested, tweaked, and tuned by our tuner shop. At least this time hopefully we will have all of the previous problems handled. The fuel system is up to par, the plugs are brand new, O2s are new, all of the engine sensors now are new, and the gearing is such that they can do their pulls in 3rd gear instead of 2nd.

    I know this can run like I want it to - it did for a couple of drive cycles after each tuner worked on it. Then it somehow "unlearned" the tuning fixes and went back to the bad idle, the bad running, the rich air/fuel ratios. Took it to the tuner March 13th and we'll see what they can come up with.

    WHAT'S NEXT?

    I'm getting tired of daily driving in the F350 1 ton, but it is a nice truck - just too damned big. My little short wheelbase 1/2 ton is much more enjoyable for tooling around town, taking parts to and from suppliers, and motoring through traffic.



    We have a number of items inbound for the next round of mods like the helper bags and compressor. I need to research the fix for the fast blink as well as find some proper/matching color temperature LED bulbs for the main headlights. Finding a supplier for our custom 20x11" wheels is still a struggle and some recent changes at Forgestar/Momo have left me hanging. There are some rear swaybars we are looking to add. And the Sparco seats and belts is a project we're pushing back a bit, as that could be a chunk of work. I will post up soon after our the round three of dyno tuning, hopefully with a solid running engine and some "after" 0-60 mph acceleration test videos.



    At the same time that this GMT800 thread update was posted, we wrote and published another update to our shop's E46 endurance race car in this long term E46 development forum build thread. You can read that here.

    Until next time - thanks for reading!
    Last edited by Fair!; 03-24-2020, 07:52 AM.

    Leave a comment:


  • Fair!
    replied
    continued from above

    TRANSMISSION + STALL CONVERTOR UPGRADE

    One of the issues we noted to the tuner shop that does our custom tunes, and that they noted as well when working with it in November at the dyno, was seemingly related to the transmission. When it was in Drive or Reverse and you applied the brakes at a stop, the engine would die. We had already swapped in a new trans pan (the black one below) and filter into the original 237K mile 4L604 automatic when we put in the 347 in October 2019.



    Our guys had noted that the shift selector switch on the side of the trans was GLUED into the mating harness connector when they removed it to do the 347 install. So the selector switch (above left) and then the mating connector (above right) were both replaced - at two different times - with no change in the issue.



    The engine was still going dead when depressing the brake at a stop, when the trans was in Drive or Reverse. Made it a real chore to drive! The prevailing theory after 3 different tuners looked at it was that the torque convertor was some how mechanically locked up and putting too much load on the engine at idle when in gear and the brakes on. And since the bands were slipping on the 237K mile 4L60E trans before the engine upgrade it was a good time for an upgrade.



    Back in December 2019 I had taken this 4L60E core trans and convertor from the 1999 GMC to a shop who specializes in upgraded transmission rebuilds. They built it for the 500 whp "stretch goal" we had in mind, with a custom built ~2800 rpm stall convertor using the OEM lock-up style unit. Kind of their "Stage 2" trans. We were out of options, time to install this in January of 2020.



    Our shop schedule was packed and we didn't get the truck on the lift until Jan 21st to get the old trans out (above left) and the built trans and convertor swapped in (above right).



    Instead of the bargain brand trans fluid we went with Motul ATF VI this time, 12 quarts - with about 2 added to the convertor before it went in. Went to go drive the truck... no difference. So it was time to call in yet another tuner, who diagnosed the issue looking at real time data via HP Tuners. He noted the brake light switch was actually triggering a total lost of ignition advance when in "D" or "R" but not when you selected Park, Neutral, or "2" on the gear selector. This was wacky!

    We had 3 different tuners look at this and each one found a work-around... but the changes never lasted more than 2-3 drive cycles. Then it would start the same nonsense.

    BIG SUSPENSION CHANGES

    During the time between the first dyno tune in November and the second attempt in February, we did a LOT of suspension changes to this truck. What I hoped would be a simple bolt-on set of upgrades that actually dropped the ride height by the advertised amounts was very much NOT the case - nothing was easy and nothing matched the drop heights claimed. What I had wanted to be a 4/6 drop ended up being a 7/6 drop, before we made some custom parts to raise the front up... and we're still not 100% done.



    FRONT SUSPENSION CHANGES - ROUND 1

    Let's start with the front suspension here and I will cover the rear on a section below. I won't go into all of the research we did into choosing the brand of drop spindle / shocks / swaybar upgrades, but just know that it was extensive. I've been burned by some truck suspension upgrades on other trucks before and steered clear of certain brands. The final option was far from ideal but we "fixed the glitch", eventually.




    I chose what I thought was an industry leader - Belltech - for a drop spindle and matching spring for a supposed 4" front drop. This was most definitely NOT a four inch drop kit, as we soon found out.



    The spindles looked decent, as did the included front spring. We weighed both, because that's what we do, then Jason rated the front spring on our digital spring rater.



    What was claimed to be a 940 #/in rate was actually closer to 975 #/in, but that's not terribly far off. Really big rates due to the inboard mounting on the front double A-arm suspension.



    The "Two inch drop" spindle showed significant differences in the placement of the hub, then the packaging included with the kit said it was a 3" drop spring. Should have been 2" + 2"... but maybe the packaging was just incorrect.



    After the brake caliper, rotor and front hub was removed, Brad used his bag of tricks to remove the front spindle and spring, pop loose the steering tie rod, then the upper control arm was pulled off as well.



    The Bilstein 4600 monotube dampers we installed last Fall were kept, as were the front hubs (which felt tight). A pair of new front ball joints were sourced, which press into the upper control arm.



    Per the instructions from Belltech, the forged steel upper control arm needs to be "flipped" 180 degrees to work with the lowered geometry and spindle. To accommodate the flip, the upper ball joint hole has to be chamfered on the opposite side, then the new ball joints were able to be pressed in fully.



    The OEM lower ball joints bolt to the lower control arm with 3 bolts and go in from the top of the lower spindle opening. The threaded stud sticks out of the bottom of the spindle, as shown above. Due to changes in the drop spindle length the stud would contact the inner barrel of a 17" diameter wheel and might not even clear an 18" wheel.



    So the procedure shown in the instructions - I kid you not - is to cut most of the stud and nut away, as shown. Once you verify clearance to your 17" wheels like we did, you Loctite and stake the nut to prevent it from backing out. Yes this seems a bit sketchy and we are going to be watching this like a HAWK whenever the trick is driven a bit and comes back in. Eventually, when we have a proper set of 19" or 20" wheels we will buy NEW front lower ball joints and swap those in - and keep the full length stud and nut, which will clear the larger diameter wheels.



    After both sides were completed the car was lowered down and - it was not a 4" drop, it was a 5.5" drop! (we had before-after measurements, of course) It was tucking the front tire so much that the tread was hitting the fender at full lock. Not good at all. We began calling "Belltech" tech support at this time...

    REAR SUSPENSION CHANGES - ROUND 1

    We actually tackled the rear suspension drop before the front, which is why we have this wacky shot below.



    This was done with a "matching" Belltech "Six Inch" drop kit in the rear. The 4/6 was the look and height I wanted, but it didn't turn out that way back here, either.



    What we ordered was this frame C-notch kit and axle flip kit, which provides more clearance at the frame for the axle and moves the axle on top of the rear leaf spring mounting for the added ride height drop.



    You can see the before (above left) and after (above right) with the C-notch and axle flip completed. At that point we still had the stock length rear dampers.



    The C-notch install isn't "hard" but it is time consuming and requires some tools and skills - and a lack of fear. Evan used the outer piece to mark the cut, then cut the frame with the 90 deg die grinder and a 4" carbide wheel. Then the piece was clamped in place to mark and drill the holes from the reinforcement.




    Some weld-thru primer was used to coat the frame (which is bare steel - don't ask me why) after the notch and holes were completed. Then the reinforcement was bolted in place, along with the inner wall section (it is a "box" around the frame)



    This isn't a modification that is easy to un-do, with the giant notch cut out of the frame. So we went ahead and welded this reinforcement in place, as well as bolting it. This is why we did the weld-thru primer was used in an earlier step. After welding the ends were painted semi-flat black, to match the powder coated kit.



    After the C-notch was completed on both sides it was time to "flip" the axle from underneath (above left) the leaf springs to on top (above right).



    The included bracket (above left) ties into the bottom of the leaf spring bracket welded to the rear axle, and gives it a flat face to sit on top of the spring. The included U-bolts clamp the axle to the leaf spring on both sides. The boxed section of the frame reinforcement is shown above right.



    There is also a bump stop added at the C-notch for the axle to touch, shown above. And the rear shocks came with a pair of extension / relocation brackets, but they only altered the angle of the rear shocks, and did nothing to accommodate the length of the OEM rear shocks. We're going to have to order shocks for the back.



    The rear ended up 5.5" lower than before, based on measurements from the rear fender lip to the center of the wheel, from before/after measurements that we did on this truck (and every vehicle we work on).

    OVERALL IMPRESSIONS AND COMPROMISES

    So apparently picking the Belltech 4/6 drop kit was a bad idea - the front dropped considerably more and the rear a tick less. This is TOO LOW.



    There were also a number of compromises we weren't prepared for, and unforeseen consequences that led to many other new parts needing to be bought/built, and installed.



    The custom twin 3" exhaust that worked well on the 99 GMC did not work on this truck when the axle was flipped. Normally the two exhaust pipes shown (above left) would be 1/2" away from the bottom of the bed. Instead they were being pushed down by the relocated axle.



    Can't really blame Belltech for that as we ran a pretty non-standard exhaust routing before. After we looked at the layout it was determined that cutting the extended exhaust tips off (dumps) was the solution. WOW it was loud! This wouldn't last long. At this point it was January 24th and the truck needed a tune, so while we were waiting for the tuners schedule we ordered some parts and made some changes.

    FRONT SUSPENSION CHANGES - ROUND 2

    We tried calling Belltech support and realized - hey, they were bought by KW Suspension! And this wasn't a good take-over, as nobody we could get on the phone knew anything about Belltech products or trucks at all. We sent them data on the front springs (which were obviously too short) and they were clueless. "We can RMA those spring" but they were just going to send us the same part number back, so that was no help. It was time to take matters into our own hands.



    We could have played the "let's order some longer springs and test" game, but I liked the ride quality of this 940#/in spring, it was just too short. So we started by taking out the Delrin spring spacer that came with the kit, which was to replace the OEM rubber spring cup. After measuring the OEM piece was no taller, so it was time to make a spacer.



    Luckily I have a really smart crew and CNC machines. Jason designed this spring spacer using some 6" round Aluminum 6061 billet bar stock we have on hand for our camber plate spring perches. Myles cut one out on the CNC lathe and it had a raised inner lip so that the Delrin spacer that came with the kit would nest inside.



    It was a big chunk of metal (ended up being 1.214" thick) and it was swapped into one side for us to check ride height. Then we made a matching one and Brad installed that above the spring on the other side.



    We also installed this Energy Suspension swaybar bushing and end link set, to replace some rotted OEM rubber bits. Brad tweaks this bushing set so the swaybar rotates with "pinkie effort" and greased the bushings at the included zerks. Jason had looked at aftermarket front swaybars but the OEM bar is HUGE! There is no rear bar, so we will add something in a future update out back.



    That raised the front up just the right amount and the tires no longer contacted the fender liner during full lock steering. It was almost perfectly level at this point and I was happy.

    SECOND DYNO TUNE - ISSUES STILL EXIST

    The first tune at True Street Motorsports in Nov 2019 was cut short due to the fueling issues. After getting the suspension changes done, the exhaust wrapped up, injectors and fuel pump in, and a half dozen other small fixes we had a scheduled slot for a 2nd tune on the dyno, Feb 19th 2020.



    They still had to make the dyno pulls in 2nd gear (due to the tall rear gearing / high wheel speeds) but at least it pulled all the way to 6800 rpm. The lambda (air:fuel) looked safe and Archie got the tuning dialed in for timing with 93 octane. With SAE correction it was making 336 whp and 341 wtq. Still 20 whp down on what than this engine made before in another chassis, but there were still issues and he shut down tuning a bit early. Making pulls in 3rd gear (1:1) would show a higher, a more accurate number - so it's probably not too far off.



    You can see the first Nov 2019 tune (and 4000 rpm die off) superimposed with this Feb 2020 tune on the uncorrected graph above. They were the same until about 4200, when the stock injectors and fuel pump gave up the ghost. This uncorrected graph shows higher 346 whp / 351 wtq numbers on a nice cool, dense day. The air fuel ratio looked good, the spark timing was spot on, but driveability was still junk. Archie noted that when he stepped on the brake the engine wanted to die.

    continued below

    Leave a comment:


  • Fair!
    replied
    continued from above

    INTERIOR WORK

    While the truck was down for the engine swap we were simultaneously tackling a number of other projects on the interior, suspension, and wheels.



    The stock interior was never "deep cleaned" on this 2000 like we finally did on the 1999 GMC, just weeks before it was totaled. So while the truck was in the shop for the engine work it was a good time to yank out the front seats and all interior panels and chase down some leaks, stinks, and test some new seats.



    Brad got the carpet then this jute mat removed from the truck. The spilled coffee and Coke stains were easier to access with the carpet out of the truck, and a pressure washer at the coin-op car wash got most of that funk out. The still wet carpets were brought back to our shop then the wet-vac shampoo machine was used with detergent and hot water to get the rest of the stains and smells out of this carpet.



    There were some other repairs done before the carpet went back in (see below), but when it did it was a night and day difference. All smells were finally gone, and we had a fresh slate to start with. I used to be better about doing this right after buying any used vehicle - I have got to make this a part of the first week of ownership for any street car that wasn't purchased brand new. Brad cleaned up all of the plastics when he was done with the carpet install, as shown above.

    THIRD BRAKE LIGHT REPAIR

    One of the reasons the interior needed to be cleaned was because it smelled musty - because there was a leak into the cabin that showed up when driving in heavy rain. I could see water coming in near the back of the headliner at the back window, near the middle. Only one place that could be coming in...



    It didn't take Brad long to see the source of the leak - the new LED 3rd brake light we added installed in 2017. Apparently the OEM unit had been out and replaced but some sealant residue wasn't cleaned off well and it leaked past the gasket on the new unit.



    With the old sealant cleaned off a new bead of clear RTV was applied around this housing and it was replaced - hasn't leaked a drop since.

    SPARCO SEAT - TEST FITTING

    The single cab GMT800 trucks have very few factory seating options. Manually adjusted full bench seat (I guess - haven't seen this) and the manual adjusted "split bench" with the combination jump seat/arm rest/console in the middle.



    Both my white 2000 Silverado (above left) and 1999 GMC Sierra (above right) single cab GMT800 trucks had the latter. The 3rd "jump seat" has been used one time in all the years I've owned both trucks, and it is hardly roomy. The console is unusually small and the backs/lids break easily - both trucks had the factory console lids replaced.



    You can see how narrow the jump seat / console is in the pic above left. The above right pic shows the integrated shoulder belt and lower receiver that is part of the driver's and passenger's seats. It took riding in the passenger seat in this truck and somebody else driving to realize how "blown out" the stock driver's seat was. It's like sitting on a board, and makes long drives unpleasant. They are also the opposite of "sporty" seats.



    As part of the build-up of our shop LS swapped 86, that will be both street and track driven by my wife, we purchased two new Sparco "Tuner" seats shown above. These are both tilt back seats with aggressive side bolsters for shoulders, chest and legs and shoulder harness pass-thrus. We are a Sparco dealer and have their racing seats in all of our shop owned race cars. The traditional fixed back racing seat is less than ideal for street use, for a number of reasons.



    As part of the test fitting of the seats in her 86 I sat in both. The Sparco R333 (above left) comes in one size and was about 20% too short for me - my shoulders completely covered the harness slots, so that won't work safely for me on track with 6-point belts. The Sparco Chrono (above right) comes in two sizes, and I bought the wider "Large". It was actually a tad big for me in the waist, but otherwise was very comfortable. I really liked this seat.



    During the interior clean up, when we had some interior panels out of the way, we mocked-up the Chrono seat and I gave it a "test sit". The stock seats sit in a rather tall riser / slider, so we propped this up a couple of inches. Might have to come up a tad more, but I could daily with these easily. And it would leave room for a PROPER center console that could hold more than a handful of pens and some papers, like the 3rd seat does now.



    You may have noticed a seat belt in the "test sit" pics - that's because I purchased these MIL-spec 3-point belts from a Hummer, per Jason's research. These are used in custom applications for retractable 3-point seat belts. Will we install this Sparco Chrono seat? Well it is complicated - mounting the shoulder harness retractors will be tricky and involve some custom brackets/anchors behind the plastic interior. Myles looked at that while the interior was out.



    It would also require a custom seat base and slider - but we make those for a number of chassis now. To be able to run real 6-point harnesses would require an unusual 4-point roll bar, but that isn't out of the question either. We're looking at this in the future, but I liked the Chrono so much I bought the "standard size" so there are two sitting here...

    20X11" WHEEL TESTING (STOCK RIDE HEIGHT)

    In the September 2019 post I teased a 315/30/20 tire I had found, after hours of looking at viable tires to build this truck around. Jason and I went back and forth trying to find the perfect tire height for gearing, ground clearance, and looks. That led us to a handful of tire sizes, and the more I looked at 18" and even 19" diameter wheels on these trucks, the more the 20" diameter wheel "looked right" for the size of the wheel openings. The problem is the available wheels in 20" were all fairly narrow - the 20x9" wheel set I had on #TruckNorris was as big as they come, but it had SO much room to spare. Anything wider was a "BroDozer" wheel that poked out past the fenders - which I want nothing to do with.



    Again, as the owner of Vorshlag I have a hard time driving "just normal stock" vehicles. Everything we own has some mods, and sometimes a lot of changes - to show off the engineering, fabrication, and suspension work we do. Now I am mindful of the engines built at HPR, where I am a partner - hence the built 347" LS upgrade done here. Custom WIDE wheels is something we have been known for for many years, so why not apply that thinking to this truck?



    Forgestar said they couldn't make this with any existing flow formed "blank" or multi-piece wheel in their catalog - unless I was willing to order a LOT of wheels at once. I wasn't sure this would even fit, and I wanted ONE test wheel first. After calling dozens of wheel makers and striking out on 6 x 5.5" bolt patter custom wheels we found Mobsteel - also known as Detroit Steel Wheels.



    They made this 20x11" steel wheel with a custom offset that Jason came up with after taking extensive measurements. It took about 5 weeks to arrive, and it is a simple 2-piece steel wheel with the center welded to the hoop at the offset we requested. They make this 6 lug pattern in a number of styles, but we got the "plain" center since this would not ever see actual street use. It was the right size for the 315/30/20 I wanted to run and as you can see above the 315mm tire fit well. It was NOT a wide tire squeezed onto a narrow wheel, like I see so many truck users do.



    Steel wheels aren't known for being light, which is why almost all motorsports uses cast, flow formed, forged, or multi-piece ALUMINUM wheels. Or even magnesium or carbon fiber, but those can have longevity issues. And yes, this Mobsteel wheel is REALY FREAGIN HEAVY at 53.2 pounds, wow! That makes for an 87 pound wheel and tire.



    Notice the weight of the stock wheel and tire, or especially Forgestar 20x9" shown a few pics above at 25.6 pounds - the Mobsteel wheel literally weights TWICE as much. That amount of heft has to be accelerated from a stop, braked from speed, and damped over every bump. That's a DEAL BREAKER for me, sorry. But it can serve as a mock up wheel to test the offset and fit.



    And that it did - we put this on the truck at the stock ride height on both ends and it fit. But the 28.7" tall tire looked a bit goofy at the stock ride height, compared to the 31" tall tires that came off. Imagine how wacky the 305/30/19 (26.2" tall) or 315/30/18 (25.5" tall) would look on this truck at this height, though.



    This offset and size worked amazingly well up front without any spacers or tricks. It even steers to full lock with just slight interference from an ABS speed sensor bracket on the upper control arm. With that relocated it worked perfectly.



    Out back it also fit great - and that was a tight fit between the leaf spring and fender. We wouldn't fit 5mm more tire under that fender, no way without poke. This is a MAX fitment tire, and it uses the same offset front and back so you can rotate tires front to rear.



    This meaty setup fits even when lowered 5.5" up front, which I will show below. After that "lowered" test we had planned on next taking this offset and size and having Forgestar make a run of these for us - at great expense.

    In early 2020 Forgestar upped their prices for bespoke wheels, so that is putting a big wrinkle in our plans. We are re-assessing options now - if people would buy the many sets we have to custom order, then the bespoke upcharge won't apply. It is a risky investment in truck wheels that we aren't known for, you know?

    FIRST DYNO TUNE + FUEL SYSTEM REPAIRS

    In late October 2019 we had the truck running well enough with the new 347" LS to test systems for leaks, get the electric fans wired in, but it wasn't driving well at all. The cold start was garbage and the engine would not idle at a stop when in Drive. After it warmed up it was a little better, and I took it to a local gas station to top off the tank with 93 octane before heading to the dyno.



    Kept the hood off for the maiden voyage to be able to see any steam, smoke or issues first hand, and it went ok. I had to pop it into Neutral every time I came to a stop, but figured it was "in the tune". We scheduled a dyno tune (they get booked up weeks in advance) and took the truck in the first week of November.



    The tune did not go smoothly and they noted several limitations in the stock fuel system. As I had feared, the stock fuel system was running out of steam above 4000 rpm at Wide Open Throttle. The 19#/hr injectors were at 100% duty cycle early, which is why the Lambda above goes lean. Also the stock 90 lph in-tank fuel pump was out of flow and the engine started falling off early at 4000 rpm.

    There were several other issues: The wheel speeds were so high in 3rd gear (3.08 final gearing would have made for 160+ mph) that this dyno pull had to be done in 2nd gear, which "hides power" - not to mention that this engine should pull to 7000 rpm and make peak power around 6500. It was just getting so lean above 4000 he had to shut it down early.



    Jason and I researched the injector options and calculated how much fuel pump we needed. We could have adapted a 255 lph Walbro pump to the stock pick-up / sender unit, but that had 237K miles on it. Instead we ordered the Walbro TU434HP drop in replacement above. This Walbro unit is shown as a 190 lph pump in some literature at 255 lph in others. Either number was more than enough for the 400 whp goal we had for this truck.



    We had the bed off for other reasons and that made the pump install very easy. This was a simple drop in, no custom work needed - which was nice for a change on this truck.



    I was already in the middle of some other costly upgrades on this truck (shown below), so I was looking for a cost effective upgrade for the injectors. Calculations showed that these 31#/hr OEM injectors from a Gen IV truck 5.3L (that a buddy sent me to try) would work at the power levels we projected, but they needed an adapter to fit the fuel rail and wiring harness connectors in this 2000 era truck. The above right pic were not the right adapters - it was the reverse of what we needed, my bad.



    I researched EV6 and EV1 injector bodies and plugs and ordered this set of ICT jump harness adapters. That actually fit these 31#/hr injectors and our truck's engine harness. But after several hours of attempts and testing, they simple did not fire these injectors or flow any fuel. The engine would not start, and I could never smell fuel in the exhaust. After checking these adapters with Noid lights (which did "blink"), it was determined something wasn't right with the injectors and/or the programming. The injectors came from someone I trusted, and he had them cleaned and flowed before they were sent to us by an injector shop I have used many times.



    By this point it was mid January, and we were wrapping up the other mods on this truck - it was time to get it RUNNING and back to the dyno. So I looked at what we could get direct from DeatschWerks, and these 60 #/hr would be more than enough for this 400 whp goal and any other plans we might have "beyond that". These are a somewhat discounted brand of aftermarket Bosch motorsports injectors that we have had mixed results with in the past, but I ordered them. And with the right parameters programmed in, they fired right up and the engine ran. But we still had issues to test before it went back to the dyno tuner.

    continued below

    Leave a comment:


  • Fair!
    replied
    Project update for March 21st, 2020: We have been busy working on the #ShopTruck since the last update here in September of 2019 - we have a LOT to share this time. The ride height is a lot lower than before: a drop spindle and lowering spring up front + axle flip, c-notch and custom shocks out back. We completed the built 347" LS swap, radiator upgrade, electric fan conversion, an upgraded trans + stall convertor, custom remote reservoir rear dampers, 3.73 gears, Auburn Pro limited slip, tackled some interior work, LED bulbs, 20x11" wheel testing, lots of tuning trials and tribulations, and more. You might want to get some snacks and something to drink - this is a huge project update!

    FORGED 5.7L LS ENGINE UPGRADE

    Last time I talked about this 347" / 5.7L long block, that Erik of HPR built for me over a decade ago. Due to some mistakes on my part, this engine started life as a 4.8L iron block truck engine.



    This engine was disassembled, bored .125" over, and a "5.7L" stroke length LS crank + forged internals were swapped in to make it an iron block 5.7L LS - a combination that never existed from the factory. Even the aluminum 4.8/5.3L blocks can be over-bored to the 3.900" bore of the 5.7L LS, and the crank is a drop in.



    This had cathedral port heads shaved .030", a Scat 4340 crank with 3.622" stroke, LS1 I-Beam rods, Wiseco Pistons with the HPR ring package, and a hydraulic roller camshaft (224° intake / 224° exhaust). This engine made 355 whp in a previous project, but has been sitting, bagged on an engine stand for 8 years.



    Erik came by and we turned the motor over at the crank, which had no "sticksion" or issues. Evan then taped up the block and painted it gloss black with ceramic based engine paint. The proper "truck" balancer was installed, a new water pump and thermostat housing, and the 4-way steam crossover from the 5.3L truck engine that came out of TruckNorris.

    TRUCK OIL PAN - LESSON LEARNED

    While we were cleaning and prepping parts to go onto the built 5.7L engine, we re-used the Gen III truck 5.3L from my 99 GMC as well as ONE part from a Gen IV truck 5.3L (oil pan) we purchased for use in our Team Vorshlag endurance E46. Initially I cleaned up the newer Gen IV truck pan, then installed the the Gen III truck LS oil pan pickup onto the engine...



    The pickup was pushing the Gen IV oil pan "up" so far it wouldn't seal to the block, much less have the .250 to .300" clearance from the pick up screen to the bottom of the pan (which we check with clay). Evan noticed this and we started checking the pan depths.



    Turns out the later Gen IV LS truck oil pan (clean one, above left) is only 7-1/4" deep where the oil pump pick up sits. The Gen III truck LS pan (dirty one on the right) measured at 8" deep, which was what we needed. So I had to take that dirty Gen III pan to HPR and have it sonic cleaned, to match the look of the cleaned up front accessory brackets other parts from the old Gen III 5.3L truck engine form my 99 GMC.



    The picture above shows the Gen IV pan, which we later changed for the Gen III pan, but also shows all of the parts we cleaned up for this engine. This included the (Gen III) oil pan pickup, valve covers, fuel rails, flywheel, power steering pump & pulley, A/C bracket and alternator/power steering bracket. Most of these parts came off my 99 GMC 5.3L long block (which we showed coming out of that smashed truck, last time) and everything was COVERED in grease, grime, and oil. It took me some hours using the aqueous hot parts cleaner then the ultrasonic cleaner to get them all this clean.



    With everything cleaned up Evan got the longblock and accessories all bolted up. The oil pan and valve cover gaskets were replaced as were the idler pulleys and water pump. We re-used the alternator from the 5.3L and installed a brand new OEM replacement balancer. The last picture above shows the Dorman truck intake mocked up, but it still needed some clean-up work.

    INTAKE MANIFOLD UPGRADE

    We went back and forth on what intake manifold to use. Buy a Fast LSXR-T and then a 102mm throttle body, but that would then trigger the need for new fuel rails, cold air kit, and more. Then we looked at the Trail Blazer SS (TBSS) intake, which is the best of the OEM LS intakes, but that also required a 90mm TB, fuel rails, and more. Any of the LS2 / car style manifolds would not allow the throttle body to clear the drive accessories.



    I settled on this Dorman 615-183 truck intake made for the 1999-07 5.3L and 6.0L engines. At only $230 brand new from RockAuto it was hard to pass up. I refuse to use an old, nasty intake that is full of oil and grime when it is impossible to disassemble, to be able to clean it out properly.



    This Dorman is a new 3-piece intake manifold design that we can unbolt and pull apart - to clean or to "port", if needed. More importantly it is CLEAN - getting an old, oily intake clean again is more work than you think, especially a 1-piece OEM style unit. There are rumors that this one has some internal improvements, but without cutting open the old OEM unit we won't know.



    The base (above left) includes cathedral style ports and a 78mm throttle body inlet. I was hoping to be able to at least move to a 90mm TB, but I couldn't without spending 2-4x as much AND going to new fuel rails. I didn't want to mess with that at this time, so we went with this cost effective and NEW unit from Dorman. The upper portion (above right) clam shells down over the removable "lower runner" piece that itself snaps into the lower plenum/base section - shown below.



    There is a long O-ring that seals off the upper to the base unit. The port runners don't have (or need) a seal internally, but do have some plastic rails that engage into slots. If a little air bleeds from port to port inside the sealed plenum it doesn't matter. Overall it is a pretty slick little intake, except for two casting flaws.



    The first flaw is every port has this chunk of plastic that we had to grind/sand away, shown above. Every port is the same and we showed engine builder Erik - he wanted it gone. We did the same thing to the Dorman LS2 intake - which had the same exact flaw. It's almost as if they did it on purpose, but why we cannot fathom.



    Getting all 8 ports cleaned up and matched together (using the base and the lower port sections) took about an hour with a long arbor on a die grinder and some sanding rolls.



    The same tool was used to clean up the casting flash and weird transition from the throttle body opening to the plenum. The exit of this is still a sharp edged orifice, which air does not like to pass through cleanly, but there wasn't a great way to to smooth that out. The 3-bolt throttle body flange worked with the stock 78mm cable throttle body that this 2000 Chevy needs and is wired for. I wanted to keep it simple, remember?



    With the intake manifold prepped the rest of the longblock was wrapped up. Brand new engine mounts went on, as did some new sensors. An ICT oil pan bolt kit was purchased and that was used to install the oil pan with a new gasket to the 5.7L block.

    4.8L ENGINE EXTRACTION & 5.7L INSTALLATION



    The above prep work was done in September 2019 and by October 2019 we had a few days on the schedule open to pull the old 4.8L and install the built 5.7L. One of the many reasons for this upgrade was to solve a number of oil leaks from the engine.



    After 237K miles the oil pan was leaking, the valve covers leaked, the rear main seal leaked. And of course this early 4.8L was the weakest LS V8 that GM ever put in any truck, and it was getting tired. The transmission was starting to slip a little, too.



    With the transmission removed the intake manifold came off, then the radiator, fan and shroud. Then the engine mounts were unbolted from the crossmember and out it came.



    Surprisingly this dirty 4.8L and the 99 GMC's 5.3L long blocks sold for a decent amount. What can I say - "turbo people".



    The new 5.7L long block went back in then the Dorman intake and cleaned up 78mm throttle body went on with the fuel rails from the 5.3L. New serpentine belt and some other misc bits and pieces. At this point we kept the 19#/hr injectors (mistake) and stock fuel pump (mistake).



    Along with new engine mounts we installed a new Energy Suspension polyurethane trans mount. The old mount was cracked and nasty.



    The Dorman intake is still butt ugly with all of the tubes, cables, and wires that drape over the engine. Some cheap Mobil1 10W30 oil went in and the old 4L60 transmission went back into the truck with some fresh fluid and a filter (mistake). Various vacuum lines and "T" sections that were old and cracked were replaced.

    RADIATOR AND ELECTRIC FAN UPGRADE

    After the engine went in I had an aluminum radiator that I had purchased new for my 1999 GMC years ago that went into this white 2000 Silverado.



    Since I purchased this unit Mishimoto has jumped into the domestic car and truck radiator market - I would have bought one of those. Oh well, if the random eBay part shown here fails, I will buy the Mishi.



    The radiator install was pretty painless - it all bolted in. This unit had provisions for the in-tank radiator cooler, shown above right. Evan kept the factory hard lines from the trans hooked up to this.



    One of the things that bugged me about both GMT800s I've owned was the giant, noisy mechanically driven "clutch fan" for the radiator. When we were pulled the 5.3L out of the smashed 1999 GMC (above) I had the guys look for a suitable electric fan that we might have in the shop. We had a couple of the S197 Coyote 5.0L powered Mustang electric fan assemblies - which we often remove and replace with a slimmer electric version to help with hood venting. This is a beefy electric fan that cools an OEM 420+ hp engine, so it should do fine in this truck - if it can be made to fit.



    The truck radiator is SUPER wide but the height was pretty spot on, as you can see in the first mock-up of this in the 2000 Silverado, above left. Evan noted the the bottom was easy to secure, and and we talked about some aluminum brackets for the top - which he made out of some .100" thick aluminum sheet.



    This worked pretty darn well to not only secure the electric fan, but to center the included fan shroud in front of the radiator. It isn't 100% coverage of the core, but again - it's a crazy wide radiator. In practice it actually works GREAT - it's silent and the truck has never even come close to overheating.



    Above left is a close-up of the radiator mounting, which follows the stock design and even re-uses two rubber isolators on both sides. You can see our electric fan brackets for the S197 shroud, too. Above right is the stock radiator hose - which is very long, but the weird bends put it in contact with the electric fan shroud. Hmm, time to make some changes.



    I asked Evan to cut the OEM hose and remove the two bends in the middle, as shown above left. Then he made this 1.25" aluminum tube and rolled some beads on that to secure it to the remaining pieces of upper radiator hose with clamps. With the center tube clamped to the two remnants of the upper radiator hose it worked great and help pressure without a drop of leakage.



    After Evan had the engine hooked up and running with the custom hose, he tackled wiring the electric fan into the truck. He used an existing 50 amp circuit that was unused, then put in a working high amp fuse in the spot shown.



    Using the HP Tuners software and re-pinning the main harness for the trigger, he was able to get the 0411 ECM to control the electric fan by using the factory engine coolant switch. We tested this extensively before it went to the dyno.



    After a bit of driving, I was concerned with the hose touching the Mustang fan shroud, even lightly. So we came back about a month later and Evan made this little bracket that cradles the bottom of the aluminum tube and keeps it from touching the fan shroud.

    FIRST FIRE + SMALL ADJUSTMENTS BEFORE DYNO TUNE

    We had swapped in some Taylor spark plug wires and with a new Wix filter and all of the fluids it was time for the "first fire". This happened before the electric fan wiring work above, of course.



    With a little HP Tuners work Evan had it running but it wasn't driving very nicely just yet. Evan was chasing some weird issues in the tune that didn't make any sense.



    The exhaust sounded really good with the ARH 1-7/8" long tube headers and the custom dual 3" exhaust from the 1999 GMC. This was a setup we built in about 2013 with catalysts up front and chambered Magnaflow mufflers that exited out the right side of the truck. It was bearable on the 99 GMC's stock 5.3L but actually pretty damn loud on this 5.7L engine with a big cam.



    This work shown above wrapped up on October 30th, 2019. The engine fired up and ran, but needed a tune in a big way. There was something funky going on where the engine would die when it was in Drive or Reverse, but we assumed it would all be cleared up in the custom tune by a shop we use for these engines.

    continued below

    Leave a comment:


  • Fair!
    replied
    continued from above

    "BIG BRAKE" UPGRADE

    This is a bit of a re-hash of work we did back in November of 2013 on the 1999 GMC, earlier in this build thread. I will quickly recap the what and why...



    The GMT800 truck was built from 1999-2007 in a 1/2 ton 2WD configuration, as was the 2000-06 Tahoe/Yukon SUV. Between this long run and many versions many used a 6 lug on 5.5" bolt circle wheel and rotor. The 1999 GMT800 was the first truck from GM to come with 4 wheel disc brakes and 4 wheel Anti-Lock Braking System (ABS).



    Over that model run of tens of millions of trucks and SUVs, GM engineers changed a number of things: from rotor size, caliper configuration, and even changed to rear drums in later years on some wheelbase trucks. We spent hours researching this, took a gamble, and ordered the biggest rotors and calipers offered back in 2013. This allowed us to upgrade our early GMT800 to a 13.0" front disc from 12.0" (see above left) and to a wider rear rotor with a twin piston caliper (see above right) from the later 2WD SUVs. We shared this with the world back then and many people have used this data to upgrade to this "big brake" kit on their GMT800 trucks.



    We ordered red powder coated calipers from Powerstop, as well as their zinc plated rotors, which were slotted and drilled. Of course slotted and drilled doesn't mean squat on a shop truck, but the "bling" doesn't hurt.



    The rotors had worn and warped after 3 years of use on #TruckNorros but the calipers looked, fine, even the rear pads. I ordered 4 more of the "big" Powerstop rotors, mostly so they wouldn't rust as badly as the OEM iron bits do. The rotors on this 2000 Silverado were all pretty worn and warped (above right) except for one rear rotor we had already replaced.



    We found out years ago that the powder coated Powerstop rebuilt caliper kits (you are forced to order in pairs) also comes with the mounting brackets, which are different for the 13.0" rotor version we are upgrading to. The 2013 era calipers cleaned up nicely and new pads were used, along with new brake flex lines. Time to head to the rear brakes...



    One thing I did not document well on the upgrade we did on the 1999 GMC back in 2013 was the trimming to the rear dust cover. This is necessary to fit the larger caliper. The corners are just trimmed off with a cut-off wheel. Click on the above right pic for the marked detail that has to be trimmed. Basically - mock up the new caliper/bracket and it will be obvious.



    There are brake shoes that ride inside the "drum" portion of the rear rotors, which are what are actuated when you use the parking brake. They rarely if ever wear out, and this was no exception. The rotors, caliper brackets and calipers went on. But just like in 2013, the big SUV twin piston rear caliper does not have the correct matching brake pads listed on RockAuto. We fumbled around with a number of pad purchases back then to find the right one - there must be a half dozen pad shapes GM uses in this era. Luckily the rear pads from #TruckNorris weren't worn badly and we just re-used those (the "dirty" BOSCH branded unit in the above right pic)



    After replacing all 4 flex lines at each caliper (there are also two configurations up front - and luckily both work because I got one that was "wrong"), the 5th and final brake flex line was replaced (at the rear axle). Then it was time to suck all of the old brake fluid out of the massive reservoir. Nasty looking stuff. Then Brad put in some fresh DOT3 fluid and bled the whole system. The truck stops a LOT better and no warped rotors, yay!



    I've been driving the truck for about two months since all of this work was completed. All of this should have happened in 2017, shortly after buying this truck, but "life got in the way". Now with the new tires, new bushings, Bilstein shocks, and fresh "big" brakes totally transformed the ride quality and stopping power of this truck, as you might expect. Instead of a death wobble at 75 mph from before, the truck can "super cruise" at 90 mph with ease. This setup is finally getting us back to a known good "baseline" that we could improve upon.

    REMOVE FIBERGLASS BED COVER



    When I bought this truck the first thing I wanted to change was the fiberglass bed cover. This was an expensive item (previous owner spent $1429 getting this painted and installed!), and it is very handy to have, but it messes up the look of these trucks. Looks like the Termite Man's truck. I had one of these on my crew cab 2000 3/4 ton GMT800 and it can also limit what you can put in the bed.



    When you have a load that fits under this lid and its raining, man this sure is convenient. The gas lift struts make it effortless to raise and lower, there's an LED to light up the bed area, and it is lockable. But when you have a load taller than the side of the bed it becomes a hassle...



    During all of the suspension upgrades above in July 2019, Brad and I removed this bed cover. Its heavy - a two man job - but comes off in 15 minutes or so. Just takes up an enormous amount of space off the truck. I am trying to sell it for $300 locally (this won't "ship"), and it will fit the 6' bed GMT800 Check and GMC truck beds, of course.



    I've used the "soft" and "flip" covers, and don't care for them. The best of both worlds seems to be these locking, retractable bed covers that are metal. They roll up into a carousel like a roll up shop door, stored at the front of the bed. They can lock, and some are even motorized. This way you can open them a small amount or completely, depending on what you are hauling. Still gives you the same weatherproof bed area for carrying items in the rain as my flip-up fiberglass unit.

    CUSTOM WHEEL & 315MM TIRES

    I was a bit concerned that the "big" front 13.0" brake rotor and caliper might not fit inside the 17x7" factory wheels, but of course that was unfounded. They fit fine. My optimum "sporty truck" wheel and tire is not a 265mm all-season Firestone "Destination". I drive "briskly" and would really appreciate some additional tire grip (and a lot more power!)



    If you remember back in this thread on the GMC, we had a Forgestar 20x9" wheel that we had made to fit this truck in the unusual 6 lug pattern (6x5.5"). It was a wheel they normally make for the Japanese market only for an Astro van (weirdly popular there) but they had one raw set in the USA in 2013 that they thought might fit this truck. I took the gamble, had them powder coated grey, and fitted them with 275/55/20 tires. They fit pretty well, but there was so much room to spare. I couldn't get anything made wider from them in 6-lug... they just don't have the "blanks".



    I sold this set after #TruckNorris was destroyed and a buddy had them powder coated black and uses them with an even wider 305/50/20 tire on his GMT800. The tire is squeezed even worse than the 275 we used was, but he likes it and it soaks up the bumps.



    When we had the truck in for the June-July round of upgrades and repairs, Jason measured the truck for a wider tire. He was convinced that a 315mm tire would fit, based on clearance to this 265mm tire's section width. Now what diameter to use turned into a multi-hour research project for the both of us...



    After compiling a matrix of possible tire choices in 17, 18, 19, and 20" diameters it looks like this 315/35/20 size has the most options, the best height (closest to the stock 30" tire height), with both "sporty" and truck-like highway tire choices. I purchased this mock-up Pirelli to use on some wheel mock-up tools, then we can perfect the backspacing on a much wider 20" diameter tire.



    After looking at hundreds of wheel companies and models, calling dozens of manufacturers, we came back to Forgestar as the best choice. But to make the size we want in a 6 lug wheel we have to order a LOT of these. So we went on a search for one custom wheel to use for testing - and that was a whole other massive search that ranged from $1700/wheel on down. We have the mock-up wheel ordered and it should be here soon, then we can mount our 315/35/20 tire and see if our calculations are correct... then order the custom Forgestar wheel run (with either the D6 or F14 styles, shown above).

    Most of what we see in aftermarket wheels for trucks are for the "Brodozers" which want three inches or more of the tire poking past the fenders, plus the suspension all jacked up. Here in Texas it is every 3rd truck on the road - it hurts my brain!. And there are some truck drag racers on 17" wheels with massive sidewalls. But I honestly think there is a "sport truck" market out there...



    This wheel design a huge gamble, and I hope there are enough GMT800 owners crazy enough to buy this wheel. Everything we see for this "sporty truck" crowd tops out at 9" wide, and most of the lowered trucks we see are on OEM replica heavy cast aluminum wheels in even narrower widths. We might strike out with the 315 tire under the stock fenders, then it doesn't happen. But I think it might just fit, and then this big ass wheel could make sense...

    MILEAGE CHECK + NEXT PHASE OF UPGRADES

    Moving to the new shop (that is within walking distance of my home) really cut down on my commuting and annual total mileage on this truck. We moved the shop in June 2018 and below I have pics from almost exactly 1 year of the "short commute", showing only 9475 miles over that 12 month period from Sept 2018 to Sept 2019. That's about 6000 miles less than I used to put on these trucks annually.



    All of this driving is simply the trips I take around town, picking up or dropping off parts at various vendors, finishers, etc. The oil leaks on this 4.8L LS are getting worse, and to fix all of that properly would require pulling the engine... which is exactly what we are going to do. And replace the longblock, and more.



    We have another iron block LS engine that was leftover from another project that has less than an hour of track time on it. It was built by Erik Koenig of HPR with H-beam rods, forged pistons, a lumpy roller cam, rebuilt to perfection. Its an unusual 5.7L setup (4.8/5.3L LS truck block, bored .120" over, with a crank and forged internals for a 5.7 LS1) and it made "decent" power (355 whp on a chassis dyno). A damn sight better than this leaky 4.8L makes! To make all of that work in the 2000 Silverado I've been accumulating all sorts of bits like gaskets, balancer, bolts, water pump, and the like. We're going to start making this engine ready to go into the Shop Truck soon!



    We will swap over the last of the good stuff from #TruickNorris at the same time: long tube headers, our custom dual 3" exhaust, the CAI - and add a custom tune. Should wake up this sleepy 4.8L performance. Needs to have some power to justify a 315mm tire at all four corners.

    That's enough for this time - hope you enjoyed reading!
    Last edited by Fair!; 03-08-2020, 05:23 PM.

    Leave a comment:


  • Fair!
    replied
    Project Update for September 3, 2019: It has been another 11 months of mostly faultless driving in the white 2000 Silverado. The last 14 months have been very busy, with Vorshlag moving into a new shop, some manpower changes, and that means its difficult to tackle some of the bigger plans I had in mind for the shop truck.



    We have done a number of suspension and brake upgrades/repairs, measured for some very wide wheels and tires, and have some long term plans finally about to get underway. Let's catch up in this post and then talk about what is about to happen next.

    TRAFFIC CAM + WIRELESS CHARGING HOLDER

    In October of 2018 I installed this YI branded traffic camera. After the accident (where the jackass going 60+ slammed into the back of me, while I was stopped in traffic) that destroyed #TruckNorris I felt it was a good idea and I got cheap units for all of our daily drivers.



    The install was pretty quick and dirty - the suction cup mount on the windshield, plugged into switched power for the USB power. It came on when you started the truck, shut down shortly after turning off power. It worked fine for a few months then had some flashing "error" and quit recording. Need to diagnose this and fix or replace. Great idea to have one of these running, I would just skip the sub $75 units (even ones with good reviews).



    In June of 2019 I purchased a "wireless charging phone holder", which I wanted to install in place of the modified RAM holder we had attached to the dash. The RAM worked great, just had to plug in the lightning cable to charge the phone if my iPhone XS-Max was low on charge. I don't take long trips in this truck (max is 2-3 hours) but I thought it would be more convenient and always be topping off the battery whenever I was driving.



    The charger/holder I purchased was this "Squish" brand, about $35 on Amazon. It charges great but as a phone holder... meh. Kind of a pain to use with a "large frame" phone + the case I have. To make the Squish unit fit with the 1" ball RAM arm (which I changed out to a longer 6" arm, above left) I had to buy a 15mm to 25mm double-ball adapter. The RAM end is easy to tighten, but the 15mm ball/socked that came with the charger/holder kind of sucks, and made the overall rigidity of the holder/RAM mount suffer.



    After about a month of fighting the holder portion (that wasn't spring loaded and not quite big enough for this phone) I was more than happy to go back to the RAM mount, which fit the larger phone better, has an easier spring-loaded entry/exit, and secured the phone better in all axis. At the same time I moved the "Swigzy" cup holder into one of the center cup holder holes.



    This is a $12 doo-dad that I bought for another car (that had tiny cup holder openings) and it worked so well I moved it to the truck. This has expandable "ribs" that lock the taller Swigzy unit into the OEM cup holder opening. It supports a 44 oz drink cup better during hard cornering. After dumping one of my drinks in the floor board one too many times, this was a necessity. No harder cornering-related drink spills since!

    CRUISE CONTROL / BRAKE LIGHT FIX

    In August of 2017 we removed the foggy OEM tail lights and replaced them with these "Spyder" branded red LED units. I've been super happy with these units, which have a much brighter brake and tail light output then the faded OEM units did. Again - after you get slammed into from behind while stopped at a high rate of speed, you want your brake lights to be very visible.



    There are some problems when switching from incandescent to LED lighting in vehicles is: a rapid blinking mode (wasn't an issue here) or a lack of brake light circuit voltage change (that happened). Shortly after installing these LED brake/tail lights I noticed that my cruise control stopped working... I researched the issue and found that we needed some additional resistance across the circuit. The common kit includes four of these 50W 6ohm Load Resistors, which are about $7 shipped on Amazon.



    Usually each LED bulb conversion requires one resistor connected in parallel, across the hot to the ground wires. These are billed as a solution for "fast turn signal blinking" after installing LED light bulbs, but it worked to fix the cruise control on these LED brake/tails. These are not designed for working bulbs (Day time running light, fog light, headlight) and the resistors do get warm when they are in use. The trick is to mount them on metal surface by screws or steel zip ties (we have them mocked up above right with plastic ZIP ties - but they have been on for three months). They come with splice taps but Brad used some in-line butt connectors. Again, its been working for 3 months without issue.

    REMOVE BRAKES + DRIVETRAIN FROM TRUCKNORRIS

    We had some upgrades to tackle with on the 2000 Silverado and some of those required parts off of the 1999 GMC Sierra, #TruckNorris. So in May of 2019 we shoved the old truck into the shop with the tractor...



    This truck still had a fully functional 5.3L LS V8, 4L60E automatic trans, ARH long tube headers, our custom dual 3" exhaust, and our "big brake" kit using the best of the GMT800 truck and SUV brakes.



    Brad got to work removing all of the things that still had value, as attempts to sell this truck as a damaged vehicle proved fruitless. The ruined radiator support was cut away and the engine bay was opened for business.



    With the front of the truck now out of the way the 1-7/8" primary stainless long tube headers came out, as did the after-header exhaust and intake manifold. Then the motor mounts and trans crossmember were unbolted, with the engine on the picker...



    With the drivetrain removed, the trans was unbolted and the long block was set onto an engine stand. We needed these cylinder heads for another engine and project (our Vorshlag endurance race car).



    The accessory drive parts were stored in a tub with all of the hardware and everything that was removed was marked and staged, including all four brake calipers. Since the lines were old they were cut and the rotors weren't re-usable so those weren't salvaged.



    We pushed old #TruckNorris back outside and took some pictures, and I tried to sell it for even less money. No takers. Oh well, we will strip it further (looks like I need a dash panel for my 2000), remove the wheels, and load it onto an open trailer and take him to the scrap yards. Such a sad sight...

    SUSPENSION CHECK, WEIGHT TEST, & NEW TIRES

    In June of 2019 the tires this truck came with were pretty much shot. This was due to some worn bushings, blown out shocks, and just mileage. The truck was driving and riding progressively worse in the last year and it was time to see what all was worn out or broken.



    We brought the truck into the new shop and inspected the suspension, brakes, shocks, bushings, tire wear, and fluid leaks. There was a sizable oil leak (about a quart a month) that was coming out of all of the normal places - oil pan, valve covers, rear seal. We had plans to fix all of these with an engine swap, which I will detail more about below.



    The bushings, ball joints, tie rods and steering rack were all pretty tight, surprisingly. There was one pair of front lower control arm bushings (above left) that we could wiggle easily with the pry bar, so we ordered those for one side only (we have long term plans for the suspension that could replace all of this). The shocks looked prehistoric, but we figured as much (above right). We ordered some Bilstein monotubes for that issue.



    We also got a good weight check on this truck at low fuel - 4346 pounds with the iron block 4.8L LS V8, 2WD, automatic, regular cab short bed. Not too bad. Cross weights even looked good.

    SHOCK, BRAKE, & TIRE UPGRADES

    A lot of upgrades and repairs happened over about a one week period. I will split them up into groups.

    NEW TIRES

    After much research, planning, and finally a realization that there are no wheels that exist that fit the bill for what I want (see more below) I punted and ordered a set of four tires in the same size that the previous owner had installed: 265/65/17. These are a bit squeezed on the original 17x7" aluminum wheels but that worked before. I really wanted to do a REAL wheel and tire upgrade at this point but we had spent a couple of months looking for something wider than the 20x9" wheels we had on the truck before, to no avail.



    This was a decent brand (Firestone) that should last during the period while we have custom wheels made (which could take half a year or more), and be safe to drive and ride better than the dry rotted, worn out Goodyear Laredo tires that were on there. That was an easy upgrade, and long overdue.

    SHOCK REPLACEMENT

    On the original 99 GMC #TruckNorris we made a custom set of Bilstein 5100 series monotubes fit the GMT800 2WD chassis. It involved custom spec'ing some shocks, changing the threaded ends, bunch of work. This time we kept it simple and ordered the 4600 series Bilstein monotubes, which are made to bolt on to this chassis without any modifications.



    These still have massive 46mm monotube pistons, which are about 230% bigger than the pistons inside the more common twin tube shocks (like these old Gabriels that were on the car). The larger piston makes for better control at low shock velocities.



    The front shocks have a threaded "pin" upper with a "T-bar" style lower eye. They are mounted inside the coil springs on this 2WD truck. Removing these is relatively easy - with the truck on the lift, the suspension is compressed slightly...



    This allows you to remove the top nut (an impact helps) and then the two lower mounting bolts. The shock then slides out from underneath. Replace it from the same direction. There is a 2-piece rubber upper shock mount bushing that goes onto the upper "pin", with one bushing/washer above the upper mount, the other bushing/washer from underneath. The T-bar lower mount bolts to the bottom of the front lower control arm.



    Out back both shocks are "eye" mount style, with a thru-bolt that goes onto brackets at the chassis from above and onto the axle from below. The shocks mount in opposing directions, which supposedly helps control axle hop. Lift the axle to remove load slightly, remove the bolts, swap 'em out.

    CONTROL ARM BUSHINGS

    The front control arm bushing swap is considerably more work. If the truck is a high mileage as this we would normally replace the whole control arm, which in the end is cheaper due to the lower amount of labor involved. Again, we have some goals in mind that might make all of these bits irrelevant, but it still would have been cheaper to replace this whole arm. Live and learn.



    Brad got the left front control arm off, which is the corner that had the worn bushings - which was allowing a lot of steering "shimmy" at about 65-70 mph. Probably a bad tire imbalance also. Now that the control arm was out is when I realized I should have bought a new arm - these bushings are a CHORE to get out!



    We don't work on trucks almost ever and our bushing extraction tools were all the wrong size. We rented these from a local auto parts store, then welded/machined/repaired the busted up set of bushing tools they brought. The hydraulic press was no use - it took an impact and time to get these stubborn 230K mile bushings out.



    After more time than I like to admit, the bushings were removed and the control arm undamaged. Now it was time to get the new bushings in...



    There's a long and a short bushing for each front control arm for the 2WD GMT800, but its obvious which goes where. Those were pressed in with the same tools and the arm went back on.

    continued below
    Last edited by Fair!; 03-08-2020, 05:12 PM.

    Leave a comment:


  • Fair!
    replied
    Re: Vorshlag Shop Truck - 5.3L SWB GMT800 (Truck Norris!)

    Project Update for October 7th, 2018: Not a huge update this time, just a few repairs on the white 2000 Silverado to cover for the last 14 months of driving. Still don't know what to call this, as #TruckNorris was such a good name for the old GMC. So sometimes I just call it that. Also sharing some plans, a bit of "thinking out loud", to show where we might go next on my daily driver shop truck.

    FUEL PRESSURE REGULATOR

    There has been a weird, intermittent starting issue with this truck since I bought it a year and a half ago. It doesn't have any problems starting up in the morning for the first time, or with restarting after it has been run for a few minutes. But if you let it sit for more than 10 minutes it would take a LOT of cranking to get it fired back up. But if it sits for a number of hours parked, it would crank and fire immediately again.



    There were no leaks or obvious issues that we could see. But then a buddy of mine with the same year/model truck had the same issue (McCall). He did a bunch of research and turns out this is common - and usually a bad fuel pressure regulator. He replaced his and it fixed the issue, so I ordered one as well.



    There are two styles of regulators for these engines, so I checked my 2000 Silverado visually and this one had the vacuum line coming off at a 90° angle (instead of straight). The part was $36 from RockAuto and it was finally here about a week and a half later (the down side to RA is the time it takes to get anything). The old unit had a bad diaphragm that was leaking fuel internally, which dumped into the vacuum port. Fuel was pouring out of the vacuum line when Brad took it off!



    He swapped on the new unit in a matter of minutes. That fixed the starting issue 100%, and the truck runs better at cruise and part throttle as well. It has since rolled 228,000 miles and this original 4.8L V8 is running smoothly once again.

    OIL CHANGE AND WASH

    I was so happy with the improvement from the fuel pressure regulator repair that we went ahead and did an oil and filter change. Old oil coming out was black, 2 qts low, terrible. We had some free jugs of 10W60 LiquiMoly synthetic and then we ordered a Wix oil filter.



    Now that the truck runs properly and I wasn't ready to ram this truck into a bridge embankment any longer, I gave it a good wash. It had been MANY months and the filth buildup on the hood shows how bad it got - I washed half the hood and shot that pic above. Damn.



    Long overdue cleaning, but its been raining steadily for months here. Never went more than a few days of sunlight this summer, other than the dry month of July.

    INTERIOR UPGRADE PLANS

    Still need to replace the door pins for both hinges (parts have been here for a while). Then pull the entire interior out and do a deep cleaning - never did that on this truck since we bought it, and it shows. A bit musty inside (might have a water leak?), and very dirty carpets, but it should all clean up nicely - like it did in the GMC. Just need time to pull seats + carpet, shampoo all of that, let it air dry for a day, then put it all back in.



    We already changed the radio on this 2000 Silverado, which came with a weird unit I didn't like when I bought it (below), for the one I bought in 2013 for the original Truck Norris.



    The current Alpine unit (from the old truck, purchased in 2013) is working fine, just has some intermittent "trouble" sometimes getting a Bluetooth connection going after startup. Sometimes it works in the first 5 seconds, sometimes it takes some fiddling to make a wireless connection to my phone. Frustrating.



    Getting access to the head unit is super easy, with the front of the dash cover that just pops on and off. And with the old GMC hanging around I've got a spare, too.

    DOUBLE DIN UPGRADE?

    The GMT800 comes with a 1.5 DIN sized radio but there are all of a sudden a LOT of 2 DIN sized touch screen radios out that have Apple Car Play, Android Auto, etc. Some don't even have a CD/DVD player anymore, and even the name brand units are sub $300.



    After having used some aftermarket double-DIN LCD screen radios lately, I think I want to add one to this truck. There are aftermarket front dash covers made for a Double-DIN install (above left) and with a big LCD screen mimicking my phone screen I will have more things to distract me while driving.



    Would like to add a rear camera, for reversing (and possibly hooking up to a trailer - more on that later). I did buy a traffic camera that I have been using, but it needs to be integrated / wired a little more cleanly.

    OTHER REPAIRS & UPGRADES TO TACKLE

    Lots of little things need to be fixed on this truck, but nothing major. Cruise control stopped working a long time ago, so we need to chase that down. And of course we still have that hotted up 5.7L LS motor sitting here. And the long tube headers and exhaust from the original #TruckNorris.



    I've got the old GMC parked at the edge of the shop's parking area on new property, off in the corner next to a Miata. This way I can keep it and the GMC can become a good "parts truck" to keep this 2000 Silverado on the road.

    The old 4L60E transmission in this Silverado is starting to get tired at 228K miles. The same unit in the 1999 GMC was even worse right before the accident. So I need to decide if I want to rebuild one of these two units and swap it in with the 5.7L LS motor? Or maybe upgrade to the newer 6L80 6 speed auto? There are some plug-and-play harnesses for making the modern, stronger 6 speed auto work in this GMT800 chassis. It would require a modified driveshaft as well, maybe more. I am researching this work.



    The suspension in this truck is starting to get a bit clunky. Just a bunch of worn out ball joints, bushings, shocks and the rest. And the brakes... bought new rotors to and we plan to swap over to the "big OEM bits" from TruckNorris, just need to actually do that. And the tires on this thing are old and dry rotted. Lots to do.

    That's all for this time. Nothing earth shattering, just normal maintenance stuff and some plans.

    More soon,
    Last edited by Fair!; 09-02-2019, 02:25 PM.

    Leave a comment:

Working...
X